hi here is a chibbi kart
….okay, so only sort of, but it’s RIGHT THERE!
I have a newfound respect for 80/20. I’m not sure why I’ve never used it before – possibly because I thought it was immensely expensive (the material isn’t too bad – 1 x 1 is on average $20 for 6 feet [1]) and heavy (which is kind of true). That whole frame came together in around 2 hours net work time, which really means like 4 hours with the amount of MITERS ADD I tend to have. Whats’s expensive about the system isn’t the extrusion, but the accessories – slot nuts, for instance, tend to be $8-10 for 50, and little specialty things like hinges or plate fasteners are way overpriced for what they are. I guess it’s like selling printer cartridges and glossy photo paper to make up for the money that selling printers doesn’t earn. Fortunately I’m in a position to generate my own random interface hardware, like the corner joists.
While a fully t-nutted plate frame of the type I typically make would have gone together faster, it would have been far more expensive (necessitating me buying 4 foot or 3 foot plates of aluminum) and not nearly as adjustable.
Here’s a closeup of the underside of the seat. I discovered that the seat mounting bracket was more like 6″ across than the 5 7/8″ specified, but all that entailed was untightening the two mounting rails and moving them 1/16″ further apart. The seat mounts are 3/8″-24 cap screws – overkill under any circumstance except, you know, the seat coming with those.
And the pedals are now mounted too. It’s beginning to look like something!!!!!!
The adjustability of 80/20 slot nuts were very clearly illustrated when I found the CAD model’s seating and foot rest arrangement was “ergonomically incorrect”. The seat is further forward than its surplus website image led me to believe. Solution? Slide the seat back 2 inches and the foot rest forward an inch or so!
The steering wheel, while still for show, is probably going to be final since I still haven’t moved on buying anything to replace it…
A closeup of the placement changes – reference this drawing. In total, things have moved maybe 3 inches further apart. While Chibikart is clearly not for anyone who is not short and Asian, I will say that this still made a ton of difference in terms of comfort.
back to hub motor work
Last time, I test wound one of the stator teeth for Chibikart’s hot-modded Skatemotors. With that in mind, I now needed to mate the copier motor stators to the center shafts.
While in the 100mm skatemotors’ original designs I had called for a plastic (3d printed, injection molded, what-have-you) hub with an integrated “key” to rotationally constrain the stator, I opted for a little bit of machining time and made some aluminum sleeves with key slots cut through them. Nothing goes into the key slot, but the idea is that the OD of the sleeve is very slightly larger than the stator bore such that pressing it into the stator causes the open slot to compress a little, also gripping the inner shaft in the process.
This worked great for 3 shafts. The fourth was…. a little special, but nothing some Loctite 609 couldn’t fix. With the operation complete, I now have four hub motors ready to wind….
….
…crap, I actually have to wind it now?
Also seen above is my choice of retaining for both the stator hub and the can bearings. Those are “low profile retaining rings” for 15mm shafting. On each shaft is an inner and outer set of grooves – the inner set is for holding the stator, the outer set for spacing the bearings exactly apart. This system is one that I enjoy so far – the design change from “weird double sided machined stepped shaft” is welcome, and makes the shaft much easier to manufacture. In fact, it’s designed to be the cross section of stock 15mm metric keyed shafting if I need to poop out a few more; the dominant philosophy being if I can make it on a manual machine in 10 minutes, it will take a CNC lathe like 30 seconds.
The center threaded bore was also drilled out for a 1/4″-20 clearance hole, since I will be bolting the shafts to my axle anchor blocks and running them under plenty of preload.
winding and characterizing the motor
I have to do this eventually, so here goes….
…wait! First, I was curious about these copier stators. They have 3 little ‘toothlets’ on each main tooth, presumably so the motor can act as a stepper motor with finer resolution than flat-topped teeth. There were two downsides to this design which makes it a little suboptimal for hub motor use – the raised ‘toothlets’ vs. the valleys between them meant that the effective average airgap between stator and magnet was larger, resulting in less poorer flux coupling (less torque), and the arms themselves were kind of wimpy and thin in cross sectional area compared to the ends of the teeth, meaning they could saturate when the permanent magnetic field and the stator field aligned (i.e. less torque).
So I used FEMM analysis software made a test winding that was representative of one phase – 36 turns per tooth, four teeth wound.
This technically doesn’t have to carry any current, so easy one strand windings were used. The magnet wire was just run straight out through the slot.
Next came the fun part:
MACHINING THE MOTOR WHILE RUNNING! Like the age-old East Asian practice of consuming living seafood, machining the motor while it runs is a….
… just kidding, this is Lathe-o-mometer. While I have done drill-o-mometer and ever air-die-grinder-with-an-R/C-car-wheel-o-mometer with previous wheelmotor iterations before, the BRAND NEW MINI-LATHE IN THE IDC MINISHOP!!! is a speed-controlled and stable fixture.
The *-o-mometer procedure is to view the back-EMF waveform of the motor on an oscilloscope while it is being spun by an external speed source. The exact shape of the BEMF, and hence the motor’s potential future torque-producing-hub-like behavior, can be deduced from the peak-to-peak voltage and the measured AC frequency. That is,
I set the scope to average a whole bunch of readings (namely 16) once the lathe spindle spun up to ‘cruising speed’, so the result is a clear snapshot of the BEMF of one phase. And….. what the hell? Why is it triangular? These things are supposed to be trapezoidal. I know a triangle is like a trapezoid with no flat top, but this is ridiculous. Anyways, the “stairstep” ripple in the waveform is the little toothlets of the stator making themselves visible.
One phase doesn’t tell me very much, besides my motor is not totally bullshit. In a typical BLDC motor, two phases are driven at any one time. So to really get the whole picture, I’d need at least 2 of the phases wound. So I did!
At first, though, I managed to wire up phase B backwards – hence creating a motor which mostly canceled itself. Oops.
That’s more like it. The measured line-to-line voltage is approximately 60 volts, which really means a differential voltage of 30 volts across the two phase leads. This problem has confounded me for a long time, but I only understood why it happens very recently – the scope treats a single-ended measurement as a deviation from zero volts, and its own ground is defined always as zero volts. So even though -30v to 0v and +30v to 0v are both 30 volts differential, the swing of -30v to 30v is “60 volts”. If I had used 2 channels and a true differential measurement (ch1 – ch2) with a common ground, then the waveform would actually be 30 volts peak to peak.
The other important number is “203.3 Hz”, which is the electrical frequency of the motor.
To convert 30 Vpp and 203.3Hz into a useful motor torque constant value in V/(rad/s), I multiply 203.3Hz by 2*pi to obtain a value in electrical rad/s, then divide by 7 to obtain a value in mechanical rad/s (because in a 12 tooth / 14 magnet motor the electrical speed is 7 times the mechanical speed). Then 30v is divided by mechanical rad/s to yield V/(rad/s), and the magical number is… 0.164 V/(rad/s) or Nm/A.
This was pretty promising – 0.164 might have been quite a ways off from the original estimate of 0.23-0.25, but at least it 1. wasn’t outright terrible and 2. showed to me that the stator teeth were not saturating all over the place.
With the motor characteristics verified, it was time to beast the windings:
Okay, I give up. Hobbyking, how the hell do you guys do this?
While I thought previously that 36 turns was a reasonable count, that test was done on one tooth, very neatly and patiently arranged, and compacted at the end. It turns out that this is not always possible to do with adjacent teeth, and once the turns pile up even a little bit, the destruction of order is very rapid. This stator shows clear signs of “hobbykinging” in the second sense – the windings almost falling out of the slots because they have been piled so messily during the process.
Really, I was able to stuff only 36 or so turns onto 2 teeth on phase A. Everything else is probably 33 turns or so – I some times could not fit the last few at all. I might have to either rethink the hex-28 gauge winding scheme or reduce the turn count officially (sacrificing Kt even more), or just have more patience while winding. We know the latter isn’t going to happen, so I’ll have to go back to playing with other wire sizes. What’s distressing is that the stator is pretty much totally filled out – I’m not sure what single-strand big wire size will get me the same level of turns.
Nevertheless, I pressed forth with terminating this stator. There’s absolutely no hope of ever installing Hall sensors in these windings, so I’m going to pray to Motor Jesus that Jasontroller can start these under load.
I once again took a page from the ICBM (Inexpensive Chinese Brushless Motor) Design Book and just heat-shrunk a section of my magnet wire pigtails to use as main motor leads. Soldering real wire inside the motor takes up previous space that I’m not certain exists in this design. The “star point” was made by running a small length of jumper wire (the red wire) between the endpoints of the phases.
And once I packed it back up inside the skate wheel, here it is back on Lathe-o-mometer and…. wait, did it get worse? Now it pumps 30 volts but at 277 Hz. That’s a performance decrement of over 36%. This is probably caused by my inability to shove the proper number of turns onto the stator in real life.
This new measurement results in a Kt of a little over 0.126. Sadness :(
The resistance of the motor from line to line came out to be about 450 milliohms – I predicted about 400, so this is good to see. However, this could still be too much – say I am running at 20 amps – I’m still losing ((20 amps)^2 * 0.45 ohms) watts to heating! The motor is not going to last long at all being a 200W heater.
But at least it sounds and looks great!
I’m probably going to pull out the Excel spreadsheet or MATLAB script and run some possible combinations of turns vs. wire gauge vs. paralleled strands to see if I can get a reasonable combination of torque production and low core resistance. However, physics constrains me significantly – as packed as the slots are, my losses on average are going to remain the same no matter what. The only thing that will result in more crank is packing more copper into the slots.
The 100mm skate wheel motors have always been underpowered for vehicle moving, but here’s hoping they work out!
I’m really digging this build! Looking forward to the next installment.
Wow
Is wonderfulllll :)
Good jog man!
Parabéns pela criatividade e tempo rsrsrs