RazEr rEvolution Repaired… with Sensorless Jasontroller

I’m sort of in love with these Jasontroller things lately, honest. I guess it’s because it temporarily relieves me from buggy controller duty and it’s already better than anything I foresee myself building in the near future.

The last time RazEr was mentioned, it was rolling on nice new wheels but with a miniature house brick stuck to the back half of the deck. That’s the sensored shady e-bike controller that I picked up in Singapore. For a while, I had bounced around the idea of just mounting the thing inside. The board in those controllers isn’t that large – it’s the aluminum case that comprises most of the volume. But I ultimately took the controller off, tossing it in the box of EV parts, and RazEr was left a dummy for a while…again. This being the semester I have devoted to making sure more of my projects were working instead of starting endless new ones, I decided to dig it out and investigate everything again.

Embedding the controller was only possible if I switched batteries to something with better packing density. The A123 26650 cells are nice, but they’re not the best if I need more volumetric energy density since there are huge gaps between the cells, even in the “close pack” configuration.

I started playing around with various arrangements in CAD and in real life. I used some spare surplus 18650 type Li-ion types to gauge just how many cells I can stuff into RazEr while either maintaining or improving my pack capacity. I could, in fact, fit a 3rd “row” of 18650 cells in the center of the frame where there is a cutout in the aluminum structure. With 16 cells per row, I could maintain a 12-series (38.4v) pack.

Testing with the Sensorless Jasontroller revealed that it handled RazEr’s hub motor extraordinarily well. It was significantly quieter and smoother without sensors, which boggled me for a while – but the sensors in the DNIR are known to be placed with some angular alignment error. Sensorless commutation also seems to let the motor run at the speed it “wants to” instead of forcing it to be hard-switched by changing sensor states, especially if those sensors are mistimed. So the decision was made to drop a 350w type Jasontroller into RazEr instead, and keep the sensored controller around for other, more mundane tasks, like Kitmotter.

The actual cells to be used are A123 18650 cells, each of 1.1 amp hours. While it’s not like one of those brand spanking new Panasonic 3Ah 18650 cells, these are much less likely to set on fire and are more tolerant of abuse, because A123 . The actual pack is roughly 1.5 inches shorter than the 26650 pack and with 4 cells in parallel, I don’t really lose any capacity.

I really like these cells, because not only do they pack better, they respond better to Angry Soldering Iron. They’re definitely much easier to solder, and I really had to exercise my touch-and-go battery soldering. The upside of making a ‘strip pack’ is the fact that I get to drop a single piece of braid across 8 cells and have a 2-cell, 4-paralle string in the end. This pack went very quickly – in fact I spent more time making those damned balance connectors.

The linear arrangement also lent itself well to routing the cell balancing taps between conductive things in order to avoid accidental balance wire deflagration syndrome.

After finishing, padding, and heat shrinking the whole thing, I got to see how well the new pack fit into the frame. The cell parallelogram is arranged such that the bottom layer is furthest forward, which gained me another half an inch or so to play with on the lower half of the frame.

A gutted and cleaned Jasontroller is also shown in its quasi-final location. I’m just going to seal the board and then mount it to the frame via the MOSFET heat spreaders.

I used the heat spreader bar as a template to drill holes into the frame such that the board was out of the way of the battery and also did not contact anything it wasn’t supposed to. 12mm long M3 socket head cap screws were used to attach the controller to the frame.

And the controller is mounted (but not sealed in Goop or anything yet). I ended up making new leads for the phase outputs since the existing ones weren’t long enough to reach under the board and out of the Hole of Wire Clearing. I laid some silicone heat transfer compound between the heat spreader and the frame, so it should have the entire frame now to warm up.

I elected to leave this 350W Jasontroller unmodified power semiconductor-wise, but jumped the shunt to 1 milliohm in order to bring the power output up to par with the DNIR’s capabilities. On a Wattmetered run, I managed to pull 1200 watts from the thing – so close enough to 1milliohm it is.

RazEr now pulls hard enough that it will almost wheelie if I’m not careful. Right now, it is almost on par with melonscooter for speed – which admittedly is a little frightening.

And the final ‘press shot’. Maybe I can even install a real switch again!

RazEr rEVolution: Concrete-wheel-be-gone

Continued from last time, I’ve finished installing the 5″ Colson wheels onto RazEr rEVolution.

This was how RazEr was meant to be. Seriously, why didn’t I just start it off with Colsons initially? While it’s still not as smooth over the average sidewalk seam as, say, a pneumatic tire, it is a marked improvement over my surplus forklift tires.

The story continues…

The first order of business after the can was completed was to install the magnets. Foreseeing another potential stray magnet spacer herding episode like the first build of the motor, I went ahead and cheated by 3d-printing a small magnet spacer thing. This must have saved at least an hour or two of diddling with little wooden sticks.

The magnets were first located using rubberized CA glue wicked into the gaps.

Next, I mixed up my favorite concoction of West System 105 epoxy with 109 hardener and a ton of phenolic fluff filler. The filler adds volume and thickness to the epoxy and prevents it from running everywhere.

Make-a-Bot has actually been instrumental in the creation of RazEr. Not only did it 3d print the entire front fork, but now it’s serving as a convenient epoxy curing oven. I set the head and platform temperature to about 50 celsius each, and left the can on it overnight. This temperature isn’t enough to damage the magnets, but ensures that the epoxy sets thoroughly.

Seriously, what did I do before this thing? It’s really in need of an update.

The next day, it was time to pop back over to the Edgerton Student Shop (where Nice Things exist) to make the internally threaded wheel locking ring. They had the only internal threading bar that I knew of…and that wasn’t broken.

This recent build should probably be entitled “Charles samples a different lathe on every part”: The machine of choice of the shop is the revered Monarch 10EE, the later type without the big round knob. It’s nice.

Maybe next time I’ll pop over to the CSAIL Machine Shop for their Hardinge HLV-H.

The internal threaded Ring of Wheel-Retaining.

I actually had to make this twice, too. For one reason or another, my motor can was turned on 22 threads per inch, not 24 like I thought. I might have just been off by one gear after looking at the selection grid from the wrong angle. Regardless, my x24 thread did not fit, so I had to cut off a chunk and start over with a x22.

And this is how it goes on.

This is actually the wrong direction – the correct direction is with the chamfer facing outwards away from the wheel. What I discovered, though, is that it will thread on just fine in this orientation, but can only make it 3 or 4 threads facing the other way before it just locks up solid. The threads are definitely not crossing, since the initial engagement is smooth and there’ no resistance for several turns. But then it suddenly becomes very high friction – not even thread lubrication helps, and I’ve definitely cleaned this thing 5 times over.

I made a thread diode. What the hell?

Oh well – another engineering pass in the form of “let’s just keep it this way” is pulled.

While reinstalling the stator, I lost control of it under the magnets’ massive pull and it ended up slamming into the far endcap, shearing 4 of 5 sensor wires. Fortunately, this happened at a point which was outside the motor, so I was able to quickly repair the broken wires.

Instead of fixing the can in a drill press vise and slowly lowering the stator into it using the quill, I just held the two. Maybe it worked for tiny motors, but it definitely does not work for a motor like this, and I could have sheared off a fingernail or broken a bone.

tl;dr don’t beast large motors by hand.

And the wheel reinstalled. Black and gray wheels coordinate with the color of the scooter better, IMO.

Pursuant to this, I stole the front wheel and fork off the temporarily defunct Straight RazEr. So here is the finished conversion, except still with its shady-e-bike-troller tumor since I have not gotten around to repairing the melontroller yet.