ORIGINAL CONTENT! The All-Around Robot Update: Roll Cake Rises Again; Dragon Con 2017 & Uberclocker

Whoa, what happened to this place? Everything’s so dusty and gross. Why is there a pile of circuit boards on the bench??

*trips over Chibikart on the ground and dies*

Hey, remember: whenever I disappear for an unexplained period of time, it’s always because I’m working on something hilarious. This time it’s extra hilarious, I promise! Obviously I’m always itching to keep everything updated here on my latest, but just like the first BattleBots build season, externalities which if broken would make other people look like assholes prevent me from saying anything at the moment. See, I don’t mind me alone looking like an asshole…

Anyways, backing up a little in life, I decided to redesign Roll Cake from the ground up following my hub drive experiments earlier. MomoCon came and went, but the Hobbyking orders kept stacking up, so I decided to roll it all in with Überclocker’s changes for Dragon Con!

roll cake

It all begins with a wheel.

Doing the drive test with the SimonK ESCs and the Multistar 460kv motors convinced me that the hub motor direct drive would work out, at least better than the previous BS I tried to do. I went shopping for high pole-count, low Kv drone motors since they’re pancakey. The plan was just to approximate wrapping an O-ring as close as I could to the motor. I ordered a few of these AX4006 motors for their combination of weight, low Kv, and high pole count.

Roll Cake is a bot which faces some packaging difficulties, since the middle of the bot has to be left pretty open for the flipper linkage. It would actually be easier in a 12 or 30lb design, since ‘noise floor’ of part sizes is much smaller compared to the bot size. If I scaled this design up to a 30lber right now, those would basically be 6″ hub motors, which is unnecessarily large.

There’s other architectures and shapes for the bot which might alleviate this, but for the time being I decided to try and keep the cheese wedge shape but  make it a little more…

…round. Remember that the flat sided shape was just an attempt at vomiting my vision of a bot that I’ve had for a while now, not making sure it works. When you ditch the need for 6WD, things get a little simpler! Even this is technically unoptimal packaging since there will be a lot of wasted space in the narrower parts of the cheese wedge. I’m basically just reskinning Roll Cake v1 and using all the same parts, since the goal is to get it driving and flipping things reliably, albeit not spectacularly, before deciding what aspect of the design to improve.

Once I had the parts placed reasonably, I started generating frame features to accommodate, such as wheel cutouts and future bearing blocks. The chassis will no longer split in the middle – that required so much extra effort to get everything to line up. Instead, I’ll be splitting the rounded caps next to the bearings off as its own print in the future.

The previous image showed the old linear slider trigger, but packaging necessitated switching to a swinging style. This means Roll Cake won’t fire when upside-down with the drum running in reverse – I’d still have to ‘self right’ so to speak. That’s fine, since I’m also ditching the double-sided linkage due to it taking up the entire center of the bot from swing space. At least keeping the flipper single-sided lets it still have structure in the middle!

The chassis is now taking shape pretty well, showing the swing trigger’s backing and “drilled” bearing cap holes and the like. I’m designing this to print ‘upside down’ on the flat top face.

After defining critical part anchor locations, I hollowed things out to accommodate the flipper linkage and irritatingly rectillinear things like batteries. Seriously, if there’s one thing this design is sorely lacking, it’s a battery worth having. I much prefer this to be 4S, but can only fit a 3S pack of adequate capacity for now.

As I model the body, I can give components final homes constrained by mounting holes and then adjust the cutouts and spacings to fit. So there was a fair amount of tuning going on at this point, including a change of wheel size to be smaller in order to shift the wheels more rearward (to give me battery space!)

After that, the fun part became linkage design. The goal is to get a linkage design which travels as far up as I can manage using the roughly 1″ throw of the cam ring, and generally has no linkage interacting at more than 45 degrees starting angle.

My insistence on a “pull” action on the main cam linkage means I have to transform the motion through a bell crank (the bottom and right side short line) to become an upward motion. Strictly speaking, I could potentially accept a push action from the cam linkage and that can directly interface with the flipper arm and move it upwards, but it would need to be designed much more heavy to stand the compressive force instead of tension (pulling) force.

 

This bell crank itself went through a few revisions in order to minimize the impact it has on the middle of the bot, the large bulkhead that runs across the two sides.

Here, I’m comparing designed linkage travel with actual part placement, seeing how much of the middle of the bot has to be cut out. The bell crank center distances and topology have also changed. The previous design intruded on the center of the bot with its full height, whereas this “T” design means only the short leg of the T pokes through the center bulkhead.

Then I decided to wrap the bulkhead around the bell crank instead of hollowing it out pre-emptively. It’s all going to be 3D printed in 50% density anyway, so no need to pre-emptively deny myself cross sectional area (which is very important to 3D printed parts)

After I was satisfied with the bell crank geometry, I made a crude flipper arm model to start out with.

The linkages will have to fold into themselves a fair amount, so I pre-emptively carved space for them before doing anything else.

The intermediate linkage is a bit of an awkward shape – here it is taking form. It has to adapt the narrow bell crank to the wide flipper linkage. I decided to do it here, and reinforce the middle of this linkage with a big flange, instead of trying to flare the end of the bell crank wider due to my desire to print it flat and have fully un-interrupted perimeters to maximize strength.

Here, see the aforementioned flange in the center of the intermediate linkage. I’ve now hollowed the flipper arm, which will be top-skinned with hardened spring steel.

The armor for this bot is quite simple – primarily Onyx in massive hollow-ish sections for the crumple zone effect, and blue-temper spring steel covering the important parts and providing access hatches.

I added a little feeder leg next to a region with unused material thickness. This will be a machined piece which is captured with nuts and flat-headed screws.

Finished and ready for printing!

I had to split the geometry first into the printable sections. I extracted the bearing cap by making a 5-sided surface box in Inventor and using a split body by surface function. Only one was needed – the other was disposed of. Other sections such as the mostly empty tail were cut off also in order to reach the print volume, and they were designed to be bolted back on.

A day later… Her’s the frame finished, printed in 3-perimeter 50% density Onyx. Ought to be plenty!  You can see where I cut the end of the wedge off and have modeled in a few tappable holes to hold them on.

Here’s a pretend-o-bot to make sure the dimensions all fit. The bearing cap was something I was particularly nervous about. I didn’t design clearances into the linkage parts to save design effort (read: I’m too lazy to make proper constraints) so some filing was needed to get them sliding freely.

Hardware installation time! I made sure to make little access ports for the motor wires, because wouldn’t that be embarrassing?

We move now to my old high school workbench down in Atlanta, which is somehow still there and in operation (maybe being 16 feet long has something to do with it). I got all the mechanical hardware installed before leaving, and decided to save the wiring for the Dirty South.

Pictured in the foreground is my new best friend: the itty-bitty-baby-offset-screwdriver-bit-ratchet. It’s McMaster part number 52725A31, and it’s positively adorable AND the only way some screws on Roll Cake are accessible at all. I designed it this way, so it’s legit, right!?

 

As usual with this thing, wiring is a disaster. The ESCs of choice are the Afro 30 Race with SimonK set up to do reversing with my usual tricks. They’re small, but not THAT small. I decided to keep the ESCs on the same side of the bot as their motors in order to reduce the amount of long wiring runs, so there’s two on the right side of the bot and one on the left.

All the motor connections have now been made, and I left one task for last before I soldered the 3-pin signal wires to the receiver….

I had to program the SimonK firmware to activate reversing and braking and my preferred goodies. I planned ahead and made this servo to tiny-clippy-jiggle breakout cable which I’ve termed “The Simonator 2.0” in order to grip the signal wires of the ESCs. While I could have programmed them all beforehand when the servo conectors were all still there, I decided I needed this cable regardless just in case I had to change something in the field, post-installation.

I brought the finished bot to one of the robot panels at Dragon Con. Sadly this year I fell off the bus and did not host any panels, but I’ll make sure that changes next time! I’m glad that recently, my Makers presentation hasn’t really been needed – in the most recent years I delivered it, the percentage of the audience who’ve experienced CAD or soldering LEDs together, etc. has grown immensely, in my opinion greater than the rate of self-selection for these things.

Here’s the linkage fully opened! Note the preponderence of little shoulder screws forming the joint pins – I standardized all of these to the same length to save myself from my historic habit of making my robots all shoulder screw nightmares.

….and now announcing my new 6lb multibot entry??? This is the head of Lucy‘s Mei cosplay, the freeze-ray dispensing Snowball. overwatch has ruined my life run away now

I’ll post some of the test videos of Roll Cake soon – I was happy enough with its performance in the garage in terms of drivability and flipping, even if it won’t prove that impressive in the box due to being repackaged test rig parts.

überclocker

We now move onto good ol’ Clocker, which has looked like this since Motorama…

Pretty depressing, eh? In the final rumble of the 30lbers, I burned out one of the SK3 4240 drive motors, so I was on the hunt for replacements, and Hobbyking didn’t have stock in that size at the time.

What they did have is a sale on their new NTM line, which had a similar size motor:

So I scored a couple of these – they were physically the same dimension, but unfortunately these motors were slightly faster again, so I was facing the very real prospect of Clocker hitting 25mph without much provocation, which could be a liability on the Dragon Con stage.

I emptied the bag of Clocker remnants to see what I could salvage and what I’d have to remachine – the answer was really basically everything minus the motor output gear :p

Good thing Clocker is legal in the new 30lb Sportsman’s Class rules enacted FRESH AND NEW this year for the Franklin Institute event in 3 weeks!

To extricate the motors, I had to disassemble the frame, which proved a little…. challenging after Glasgow Kiss gave it a once-over. There were some special extraction techniques I had to use here on this machined corner!

From the spare Clocker parts bin I extracted another section of the 1/2″-10 leadscrew and flanged bronze nut that fit it. I’d bought a few spares last year in anticipation of needing to machine them eventually, and here we are.

The bronze nut gets machined all the way down to be smashed into the bore of the modified Vex Pro spur gear. When the gear spins, the leadscrew gets sucked in and out of the nut, and its own reaction forces are taken up by the bronze bushings surrounding it. All solid, all friction, all the time, but it gets the job done.

I’d like to eventually rebuild Overhaul’s actuator in this way, except with preloaded tapered roller bearings, for #season3 whenever it ends up being :'(

 

Mate this up with new waterjetted plates that I drilled and tapped and we have a new actuator. The drill gearbox was reassembled from stock pieces from my giant decade-old (…) bag of Chinese cordless drill parts, using the original shaft which was not damaged in the fight. I have enough pieces now to straight up make two whole actuators, which is nice.

After that, I repaired the bottom plate of the bot by stitching new holes in between the hole ones. I’m not sure if I’d use #4 screws like this anywhere in a loadbearing path (which the top and bottom plates do count as) if I redesigned Clocker again, since the indirect shock loads from the 30lb Featherweight class alone (in the form of getting socked by a spinning weapon) is much higher than Sportsmans. One of the corner hits from Glasgow Kiss sheared off a half dozen of my bottom plate screws just by momentarily bowing out the frame enough.

 

While I was in there, I swapped in the spare wheels made from 60A Mystery McMaster Urethane (actually OEM’d by Forsch Polymer, the most 1997 company extant in 2017). The white Smooth-on Simpact wheels had worked well enough, so I wanted to see how these would do.

Well, everything is technically ready for reassembly!

I rememberd a much better way of taking the entire top off Clocker. Previously, it involved trying to drive the center lift shaft out through ALL of the components that were shaft collar’d onto it. This was patently painful. Unlike Overhaul’s unboltable lift towers, Clocker has solid ones built into the frame rails. It turns out if I just unbolt the outer and inner frame rail on one side as a unit (9 screws), there’s enough room to wiggle the shaft out of the bearings and pop the whole thing off.

 

Clocker was the last thing I wanted to put the Brushless Rage test units in before shipping them off for production. The severely under-geared high-Kv motors will be a good stress test for the architecture, since on the Dragon Con stage I’ll mostly be driving at low speeds and turning/reversing often.

Check out that little Onyx bracket I made to hold the units. I wanted to place them flat against the frame rail behind them here, but this arrangement kept the wiring cleaner and away from the outrunner motors.

A new waterjet-cut gear and some quality Taki-time later, and everything is now back together. I did some drive testing outside, which showed me that the Brushless Rages were working great even under duress – the gearing on the motors is low enough that the bot has trouble turning in place on a high traction floor. So here I was hoping that it would be even able to turn at all on the Dragon Con stage carpet! But once it takes off… boy does it want to keep going.

the charles and the dragon con

Welcome to Dragon Con! Have a van.

I would have loved to bring VANTRUCK instead this year, as it has been now impeccably reliable after its lobotomy and subsequent headcrab installation, but could not even begin to justify the 9 miles per gallon each way. It’s beginning to dawn on me that the kind of person who would have bought one of these things new, never ever thought about the cost of fueling and ownership. I’m not quite to that level in life yet.

Overall, this con worked out a lot differently than some of my past Dragon Cons. See, I wasn’t scrambling to finish a robot every day for once – Roll Cake’s finishing work and testing occurred before the con started. Instead of trucking around a giant transforming mechanical prop, Cynthia instead prepared a bunch of pieces for the Dragon Con art show (which as I found out was nontrivial to get into)

On top of that, it’s become more of a yearly reunion for some of the BattleBots competitors and friends who have moved around the country & world. For example, I found Lisa Winter!

The cotton candy committee has arrived.

I attempted to replicate her tattoos in the middle of talking at a panel. Nailed it!?!

And for the first time in probably over 10 years, I actually played in a gaming tournament. There was an Overwatch ruined my life run away now tournament being hosted at the convention gaming center, and a few of us essentially set up #BattleBotsPlaysOverwatch.

The house equipment was sub-par, though, so we didnt’ do too well – people who have clearly been to more than one tournament brought their own mice, keyboards, headsets, and pillows and stuff. Now that’s pro.

 

HELLO FOR I AM MECHANICALLY THEMED VIDEO GAME GANDER AT MY CURATED ARRANGEMENT OF MECHANICALLY THEMED ITEMS

Alright, you know how Dragon Con goes down. Let me spare you the details and get to some robots!

MicroBattles has grown to the point where it has to be single eliminations only and running across two arenas to keep up. I’m glad that it’s a good problem to have! However, it does mean you’re pretty much one-and-done.

There wasn’t much to do with Roll Cake beforehand except get some driving in. I decided to move the tail on the flipper downwards one mounting bolt such that it was more likely to rest on the floor – otherwise, the bot tipped abouts its wheels a little. However, it kept weight on the feeder wedge, so that was a plus.

Robot Battles features mostly local builders who kind of keep to that series of events around the Southeast. It’s refreshing to see bots which haven’t been forced to become the small monolithic dense bricks that most competitions have forced them into being. These two, for instance, are hand-bent sheet metal from Home Depot, with a hand-soldered custom motor driver inside. I honestly miss these kinds of builds.

Pool noodle wheels were fully in fashion this year, made popular by the Dale robot Noodles. Hey, they’re totally not entanglement devices. The wheels aren’t supposed to come off, just incidentally if you hit them with your spinning thing! Wink wink. I suspect this kind of thing might get roundabout-banned somehow, but on the other hand, it’s 2017 – get a reversible ESC on your weapon already!

Sheet metal everything, down to the weapon! Now this is robot fighting.

Other builders who had too much time on their hands chose to adorn their robots in….. creative ways. That’s hand trimmed and applied fake wood veneer vinyl on Margin of Safety here…

I was pretty eager to fight Noodles since it’s high ground clearance and invertibility would have made for a whole match of flips with Roll Cake.

Besides the wacky builds, you had your usual array of kit-bots and modified kit-bots.

Roll Cake was matched with Margin of Safety first, obviously a fight that I was hard pressed to win. Aaron put on the miniature vertical drum module for the match, so we went head to head trading blows. Margins having the the smaller drum advantage,  Roll Cake got flipped over and I spent a while trying to self-right, but at the time didn’t have any skids on top of the bot, so I trundled it around a few times trying to get him to flip me back over.

See the two little hex nuts sticking up from the top? That was added after this match so I could get flipped over in the rumble and maybe get back up. With the drum bouncing off the ground, it wasn’t going to get enough momentum to roll it self back over, so after a while of trying, I decided to save the effort for the rumble.

In said rumble, the drum promptly threw the rubber o-ring belt and jammed as soon as it started. Well bugger me with a #1/2-20 tap, that sure didn’t come up in testing! So I spent the whole time running around like an idiot.

I suspect that spinning up quickly made the belt stretch enough (since rubber cord doesn’t have a tension element in the middle like fibers) to jump out out of the pulley enough to get grabbed by the drum. In Roll Cake 1, the pulley spacing was far enough apart that it would have just fallen off, but this time I had to move the drum closer and so there is a lot of overlap with the drum iself.

Hey, all things considered, I walked out with a working bot. It’s now time to get serious with Roll Cake. I’m extremely confident in the mechanism now, and so it’s time for it to stop being a test jig on wheels. The weapon motor is severely undersized – if there was one design which should have a motor-in-drum setup, it’s this one! And, furthermore, freeing up the space occupied by the weapon motor might mean I could use more conventional drive motors. The hub drive worked well enough, but I still prefer the positive feel of a geared motor.

And now it’s Monday!

 

With the return of all the robotty TV shows, we’ve seen a serious and sustained rise in the audience count. The room filled up to this level well before matches began, and the line continued out the door the entire day.

An entry being finished in the pit area before matches begin! How quaint.

Lisa brought itty-bitty Tento, weighing about 8 pounds, and entered it in the 12lb class for fun. This thing was built as a “how to build a robot” demo piece. Unfortunately, it suffered a gearbox failure literally right before matches began and it was of a type that nobody else was using, so spares couldn’t be located. Sad day – maybe next time!

Clocker just needed battery charging (and the replacement of a chain tensioner block) this whole event, so I’m quite pleased.

I only ended up having two matches – one against this giant purple thing (which had radio problems at the end – notice us both running onstage to disarm it), and the second against Dale’s Pushy Grabber. This thing has been sweeping RB events (literally) with the lynchpin strategy of wiggling under your bot almost no matter what. Now, normally I offer at least some resistance to Dale, but this thing I had to approach either at a very specific angle or risk getting plowed off the stage almost instantaneously. We had 4 total matchups, in the middle of which Dale had to reattach one of the rollers and I had to replace a chain tensioner block which finally decided to wear through and fall off.

This event really showed that, much like my arena-optimzed Test Bot v4 days in the Late Aughties, wide ground-hugging wedge surfaces really are more of a liability on the stage than an asset. Notice how in the final Pushy Grabber matchup, I tried executing the same strategy, but got hung up on the edge just long enough to become vulnetable. The only weakness of Pushy Grabber right now is a long-reach forked robot like Nyx with the lifter attachment – Clocker did not have enough “stickout” to really get a good handle on it – nor did it really on other bots.

Unlike version 2 and 3 where the clamp arm reached all the way to the end of the forks, this one for the sake of looking more like Overhaul has the ‘grab point’ more inwards, so I had a harder time getting opponents into the clamp in the first place unless I took a straight run at them with some velocity – upon which I would often run into the stage edges.

I stuck around for Rumble #1 which I won by virtue of trying to get around the damn stage and mostly ignoring opponents…. and in Rumble #2, I just took the wedges off and ran around like an idiot some more, accidentally handing the win to the purple thing after doing some kind of J-turn rocket jump off the stage. Oops.

This event was also the final straw for me in terms of gearing down the drive motors more. I’ve been threatening to go to 2-stage gearboxes for the drive, and now it’s more necessary than ever. Clocker v3 was geared for 19mph and was already a rocket, and there was barely any need for it on the stage. I’ll probably move to 11:1 2-stage P60s and use smaller 35mm drive motors.

Yes, this kind of thing is legal here, with a catch: It doesn’t exceed either 500 RPM, or 20 ft/s edge speed.  It’s driven by a geared motor, so it will more lift your bot up and chew at it.

 

Replicas of BattleBots entries are the in thing right now! This is Tuskin Raider, a 12lb Razorback-alike that Jamison built. It got all the way to the 12lb finals.

This is a 12lb shell spinner.

And here we have the assembled Power Rangers shot of all the scale models. Hey, we can film #season3 right now if we just get all the cameras up really close. I keep bugging Jamison about why he didn’t make Tuskin a 30lber instead of a 12lber.

So that’s it for Dragon Con! Two working robots remaining, shenigans abound, and…. no van adventures. Wow, when did my life become routine? Obviously it’s time for another all-vans update soon….

Motorama 2017: The Event Report; Or, How Not to Scale-Model Test Your BattleBots

And we’re back! I must say, in a way, I miss the abject chaos (read: spinners) of the full-contact weight classes, but it is glaringly clear that I need to get my strategy back in shape. In all, this event was a good wake-up call for me if I want to play the BattleBots #season3 game seriously, but that’s for a later analysis. Here’s how things went down, starting with the finishing of Clocker a few days before.

One of my last to-dos was making spare armor wedges. I’d already waterjet-cut the plates, so they just needed to be cleaned and welded. These wedges represent a simplification of the design used on Overhaul that I would like to transfer. They’re simpler, reducing the number of facets and panels by half*,while also retaining the same lower-edge durability with a (higher mounted) gusset. However, they are missing the “Jersey barrier” double-angle front that Overhaul has, and this will be important later.

So there are four wedges – two are made from regular cold-roll mild steel, and the other two from 4mm AR500 plate. I’m really expecting to run the AR500 plate as primaries, and only ditch out to the mild if they get (somehow) demolished. I suspect there wouldn’t be much left of the bot if that were the case, but it’s good to have options! The 4mm plate one weighs several ounces more than the mild steel, owing to higher plate thickness (.125″ vs .140″) so I’ll definitely have to free up weight for it.

I jigged the whole thing up since it tabs together into itself and tack-welded the panels together using a TIG welder, before switching to the good ol’ spray-and-pray MIG welder to blend the outside seams together and drop a huge interior fillet into whatever edges I could on the inside. I am still the only person I know who tacks assemblies together using a TIG welder, and then switches to using a MIG welder. I write this off as me having zero patience for welding, but needing the initial assembly to be straight, so I do it with the precise near-zero-force application of a TIG welder.

*Note that Clocker doesn’t have forward- or side-facing wubbies like Overhaul, so if those features are being added back, it would increase the plate count, but still not to the point  where I had them for #season2

Free up weight? Where the hell else can I do that from!? It seems like Clocker’s been pretty well dieted, but a few weeks prior I had started thinking of do I really need semi-infinite drive power? in the form of possibly replacing the AXi motors. They work great, yes, but are definitely overpowered and therefore heavier than I need. I decided to swap to a set of 42mm SK3 outrunners, which would reduce me by around 4 ounces per motor, allowing me to use the AR500 wedges as the heaviest configuration. Power-wise, the SK3 outrunners would have been just fine. They also pair up with the pinions of the 4:1 P60 gearboxes from BaneBots I ordered (due to the higher Kv) and bolt to the motor plate with no modifications.  This is a great combo – I highly recommend it as a plug-and-play 30lber-scale brushless drive rig now.

The motors were basically the last thing to arrive before I had to leave, so I decided to hold off swapping the parts in until we got to the event.

motomumu

The following image shows the totality of the glory of America:

 

 

On Thursday night, we packed Literally All the robots into vantruck, along with a sizeable amount of tools, support equipment, and other miscellanea. I planned to get there early-ish Friday to help set up and also to aid in Antweight & Fairyweight tournament logistics. Along with me were SawBlaze and Overhaul for display at the front of the audience section.

Sadly, this trip as-photographed did not happen, but that is an entire other story that has to be told separately. Long story short, the haulage minus SawBlaze and Overhaul were reshuffled into Mikuvan. This is a great story, I guarantee you (if you stalk me on the Internet, you already know it, so no spoilers!)

Alright, so it’s like 2PM on Friday now when I get there and everything is horrible and nothing matters. Let’s swap the motors onto Clocker:

Boy, those ESCs – spares left over from Overhaul and Sadbot, Dlux 160A HV units – are now officially overkill too. That’s what happens when you make a parts-bin robot. With the motor reduction, I was able to make weight using the AR500 wedges. Also in the same disassembly service were the floor scrubber tires:

 

Here’s a better look at them. I liked how they handled in the test box – still just a little light on traction, but very predictable. I brought along the Forsch (black) 60A wheels also, but decided to run these first since the Forsch ones felt a little more stiff.

Fast forward to Saturday and….

I feel like I’m at some kind of  career fair or anime convention. The people-ocean density was staggering; this is the largest Motorama Robot Conflict historically, and the largest year-by-year growth (over 50%). A lot of new faces, probably 25% of builders, and also quite a few returning legends. It’s a good problem to have.

In the interest of not dying, the 3lbers (beetlewights) were basically running in a parallel event with an 8 foot arena just off screen to the left, with only large bots – 12lbers, 30lbers, and 30lb Sportsman’s – running in the big arena.  Given the sheer number of beetles, it was the only way!

What’s great is MassDestruction helped spawn several ‘newb-vets’ who cut (….blunted?) their teeth in the MassD arena over the course of the last year.  These are two of Alex Hattori‘s robots. At this time last year, he had a 30lber made of two steel bars welded to a cast iron pot, and since then he’s cleaned house at like, every MassD ever, I swear.

 

 

Some other remarkable bots forged at MassDestruction from guys who work at, uh, MarkForged. Crap, my sponsor is beating me at my own game! What do I do!?

Another one of my favorites return – this is Pitter Patter, a 30lb shuffler (actually 45lb in the weight class) which way back in the olden days of Motorama 2015 was the original design model for Overhaul 1’s shuffle drives, which were basically a direct knock of this thing! For this version, the saw got smaller, but the shufflers got way faster… like 3000 RPM fast. This thing was cookin’ it in the arena.

Basically, you’re not getting anywhere NEAR the whole story just from these few photos. I remember when robot tournaments were this big, from the momentum of the first run of BattleBots, and I hope I see the 2nd Great Awakening of robots progress further still.

Anyways, onto my matches! This is Glasgow Kiss.

Topologically, it’s a good mockup of the Cobalt match. This is okay too! I’d actually hoped for a vertical spinner opponent so I can practice my anticipated strategy of using the ünicorn. However, I’ll gladly try to practice my horizontal-fending tactics too. The high level plan is to come into his weapon tangentially using the AR500 wedges and bounce him around, ideally towards walls, and try to corral into corners. More or less the same plan as for when I fought Cobalt.

I mounted the ünicorn anyway in case it could be used – I wasn’t counting on trying to swipe the belt pulley, as it’s too far inwards.

So how did this match go? Uhhh…

Well that’s not very typical at all.

Let’s watch the match video to find out what happend!

Alright, so my strategy starts out working fairly well. I’d say about 0:30 is when things start going awry. While I get a few more good tangential shots in, Glasgow Kiss is able to get one or two shots in which climb up the wedges and take out the clamp actuator and main lift gear.

At 0:49 I make a pretty bad driving error and end up plowing directly into the blade, so the forks and clamp are pretty much done by then – you’ll see me raise them to try and keep them up and out of the way.

The last big connection throws both of us apart across the arena, and I’ve lost all drive power by now so I tap out.

What Andrew (driver of Glasgow Kiss) does well is pivot the bot on the blade axis – in part a consequence of it being so heavy – such that it’s hard to just ‘get around the back of’ or execute similar strategies. He does this several times to leak away from Clocker’s grasp succesfully, leaving me to chase while he spins back up.

If you watch closely, you can see Clocker has some maneuverability issues right away. One of them is the bot’s right side having a tendency to stop and not reverse, which means I missed a few in-place turns. This occurred to me as strange – I mentally wrote it off to the smaller brushless motors in the drive cogging on start, but it definitely didn’t occur in test box driving. The heat of the match kept me moving, though, and I elected to try and drive around the problem, exercising the tactics I outlined in how2brushless at the bottom.

So Clocker seemed to be in one piece still at the end. Time to appraise the damage:

Check out the gear carnage. This gear is made from 7075 aluminum. It’s a nice and rigid alloy, one of the strongest by tensile strength aluminums, but it’s really best used in bulk such as gearboxes or bearing blocks and the like, not in thin sections. The gear is fairly heavily webbed out for weight, so it cracked through readily instead of bending. A 6061 gear would have bent and I would have had a chance to sledgehammer it back to something resembling flat.

 

Glasgow Kiss machined off most of this corner here when I was turned around. I’ve thought about making plastic corner hoopy-jiggles before, but haven’t been compelled to yet. As a part of a comprehensive horizontal weapon defense strategy, it might be worthwhile to do for Clocker using some 1/4″ UHMW or a thinner spring steel.

D’oh. I think the cross-arena impact stripped all the #6-32 threads from the end of the gearbox, so I lost drive on this side. On the other side, the chain jumped between the drive sprocket and the rear wheel sprocket.

You know what was awesome though? The AR500 wedges, on both sides, are practically untouched. Lightly divoted, but they were still flat to the ground. I did write off two of the lower wubbles on each side which had some tearing damage beginning.

But you know what – this setup went head to head with one of the biggest 30lb weapons a dozen times and isn’t much worse for the wear. What it really showed me is that Clocker’s frame and armor is perhaps overly built for the weight class now that geometry is compensating up front for frame thickness.

By near complete accident I’d say, the ünicorn came THIS CLOSE to piking the pulley and belt.

Alright, it’s time to fix everything up. Both sides of the bot had to be disassembled to replace the drive motor studs with longer ones. Since the P60 motor plate screws don’t go all the way through, there was some thread left which I could use with longer #6-32 bolts.

It looks like the frame was tweaked about 1/16″ in a parallelogram shape, from a similar corner hit on the rear right side (opposite the well-machined one), so the left side drive sprockets became offset enough to cause problems.

Getting the damaged lifter parts off was an adventure that took a long time. I’m now heavily rethinking the clamp collars on live shaft approach. It was fine in the Sportsman’s class where Clocker never took any real damage there, but with everything twanged up, there was hearty use of deadblow mallets, aluminum pusher tubes (to avoid marring the shaft), screwdrivers, etc.

What I couldn’t save were the clamp actuator and lift gear. I had thought about machining another lift gear the week before, but it remained just a thought. While I had a newly assembled and painted clamp arm ready, I didn’t bring spares for the clamp actuator. Without a backup clamp actuator – since Glasgow Kiss had basically wiped all the internals out also – I had to push everything back together in “spatula mode”, just with the lower forks and around 120 useful degrees of gear. Once again showing the difference between Sportsman’s and the full contact weight classes – just like in BattleBots, you should really be prepared to build 2.5 robots, one full set of spares and another for the things which break the most often.

So I delay my next match (and run down that delay as far as I can) to get spatula mode together. When I finally hustled into the arena, though, I discovered that Clocker could only spin in place or turn right. I clearly had wired one of the drive motors backwards, but what? Moving only channel 1 in my elevon-mixed (single-stick driving, basically) radio only caused the left side of the bot to move, with no response from the right side. However, it could obviously spin in place; without a motor being backwards, it means it could drive straight forward or backwards, but only turn right with 1 channel.

Without more time, I had to forfeit my match against Shaka, who, I will point out, somehow went 2/2 at this tournament using only forfeits. It won its matches by forfeit, but had endemic electronics problems which caused it also to lose by forfeit… I am told that in testing shortly after our non-match, it blew up.

Back in the pits, it took me a little more investigation to discover that my Hobbyking radio had somehow lost a mix. When you configure a radio for single-stick driving (or Delta Wing, Elevon, V-tail, etc. for aircraft), you assign mixes to tell channel outputs to listen to certain combinations of stick inputs. Here’s what a typical simple elevon mix looks like for my Hobbyking T6A-v2 transmitter:

There’s two mixes involved – one to tell Channel 1 to move with Channel 2, which on a typical radio is the vertical throw of the right-hand joystick. This means pushing forward on the stick sends the same signal to both outputs on the receiver, so the robot drives forward.

The other mix is to tell Channel 2 to move the opposite of Channel 1, which on a typical radio is the horizontal throw of the joystick. This means if you push stick right, one side of the bot moves forward and the other moves backwards, and is accomplished by setting the mix percentage to be -100 in both directions (do the opposite no matter which direction the stick is moved)

For me, the latter mix – the one outlined in Miku Pink – was NOT responding, despite showing correctly! This meant moving Channel 1 resulted in no opposite motion, just the bot pulling right. This was exactly the behavior seen in the arena, and I would never have discovered it if I had not accidentally put a motor in backwards.

I said the maneuverability tics Clocker showed in its first match will come into play later. I’m now 99% sure that this issue affected the match, and I tried to dynamically drive through it since I try to avoid stationary directional changes (turning in place) due to the brushless drive. A non-working Elevon mix will still kind of work if you move Channel 2 first – it will simply add and subtract Channel 1’s value from one side. In this case, it left the bot prone to pulling right, which is exactly what I saw.

How did I discover this was the problem? Well, I simply had it resend all the settings to the radio without touching a single one and it resolved itself. My radio literally lost a mix from its memory between Friday and Saturday for reasons unknown, even to the point where it convinced its software that the mix was still present.

I must say, I am not even mad. This is an impressive failure mode that I’ve literally never seen before, ever. Before anyone dishes on Hobbyking radios, though, I personally have owned a half-dozen (I keep accidentally giving them to newbies or random students and then getting another one) and also worked with hundreds back in my 2.007 days when they were the radio of choice for the class, and this is the first one I’ve ever seen DROP A SICK MIX like that.

With Clocker out of the tournament and the radio issue solved (!?), I waited for the 30lb rumble to join in on, where I basically overdrove the arm past the end of the gear immediately….. so I simply ran around as a wedge corralling bots in corners until the Vex sprockets’ teeth all came off!

My chain gliders probably wore  enough in that 5 minutes of crazy driving to make the chain skip on the sprocket (since it doesn’t have that great wrap angle), and the power of the brushless drive proceedd to machine the teeth off in short order. Ah well – it was a great rumble anyway. At one point I had every bot except Translationally Inconsistent, who kept slithering away sideways, piled in one corner.

Once I find a good video of it, I shall update the post to include it.

What’s great to see is that the 60A wheels hardly wore. Obviously this is both good and bad, since it means I could have traded hardness for more traction. For the 30lbers, I might go back to the 50A compound – Clocker in previous incarnations has run 50A wheels and I’ve been satisfied. Now is when pouring a few full-size wheels for Overhaul to try and drive around would be a next step.

We part with some shots of gourmet damage from one of Jamison’s loser’s bracket matches against Triggo. megatRON was upgraded to have an AR500 impactor disc on the end instead of a saw, and having that house brought down on you is capable of some serious damage:

this kills the triggo :c

Check out the 1/8″ heat-treated chromoly-steel shell rim also, from the same weapon:

This thing is not trivial; megatRON was actually one of my more feared potential matches because I have relatively weak top side defenses. Expect potentially interesting changes to Sawblaze for #season3 perhaps?!

Speaking of which, what takeaways for Overhaul do we have here besides the obvious bring a spare of the thing you don’t think you need spares of. Or three.

  • DAMN, THAT WAS A GOOD MATCH THOUGH. Honestly, if I had the choice of losing like that to Cobalt, versus the way I did via #setscrewghazi, I’d have picked the former in a hurry. I would have had enough spares to bring Overhaul back online quickly anyway, and it would have made for a much better show and much better test of the bot.
  • I’m highly satisfied with the AR500 wedges. So happy. It deflected the hits from Glasgow Kiss with ease, and also seems to have done its job of transferring the energy into the floor. AR500 has become a bit of a crack epidemic in robot fighting recently as more of it is readily sourced along with laser/waterjet services to handle it. It’s a nice alloy, really – heat treated to the high 40s Rockwell C already, and easy to weld with conventional consumables.
  • Good deflection is also a curse, because you aren’t in control of where the big beating-stick goes afterwards. I’m more convinced than ever – besides by this hit – that the double angle on the front of Overhaul’s pontoons is an absolute necessity. I designed without them for Clocker for simplicity and to see if I’m just being alarmist, but what the single slope let Glasgow Kiss do is deflect its own way upwards and clean house in the clamp actuator. I will need to think about how to  how to retain or improve this design for Overhaul, and to add it to Clocker.
  • I think it might be time for a scoop, for both Clocker and Overhaul. You know how Overhaul has the short arms that I used against Cobalt? Imagine those becoming vestigial and ending behind a angled steel plow which could nest in between the wedges on their inside slopes, making the front of the bot more contiguous. The remnants of this design can be seen in the forward-angled plate that resides on OH1’s forks.
  • It’s more clear than ever that a self-reinforcing geometry trumps material thickness outright. If scaled down directly without changes, Clocker would have 0.75″ thick frame rails, which it clearly doesn’t. It has 0.5″ thick, heavily-machined out side rails with 1/4″ thick cross-bracing plates, and that left the match against Glasgow Kiss needing a single screw extraction and maybe a hit from a good ol’ Engineering Hammer. What this actually means is I spent much of the 6 hour drive back from Harrisburg trying to rationalize that maybe I do need to have Overhaul’s frame remachined again. I’d be able to optimize for the geometry of the side rails. It would shed a lot of weight which can go into other systems I was running out of weight for, and really, based on how deeply Overhaul’s frame rails are pocketed, it’s almost useless to be made from 1.5″ thick stock. But UUUUUUUUGGGGGGGGGGHHHHHHHHHHHH.
  • I’m really, really itching to leave the clamp collars behind when it comes to power transmission to the forks. I think when it comes to fork improvements, just adding cross-bracing to Overhaul is enough, and I way more favor the 8-bolts-to-remove-an-arm setup on it right now for serviceability. I can replace a full set of arms and the clamp actuator on Overhaul faster than I could get the damaged forks off Clocker.

I would love the opportunity to test these hypotheses on a 30lb scale again in less than 1 year, especially because I (think) #season3 is still going down this year. Even if I can’t prove my hypotheses in short order, this was all good stuff to know!