Operation ENDURING BROWN: The First Battle of Bunk Bed Hill

Alright! Welcome to another exciting episode of “Wait, when did this become a car blog? I thought it was about brushless motors!” Well, just like how I commit horrible abominations to the industry of mechanical engineering daily, here is an abomination for gearheads: If you ever wanted to mate a truck bed to a van frame, this is your moment. Because I’m about to do just that, and put it on record.

As soon as I got VANTRUCK running (even if a little off-tune), I called a convention of my somewhat automotive-minded friends. We’re like the Justice Friends of working on silly vans. Together, we will take on the challenges of…

 

Oh boy. This mess needs to be unstacked first, then we deal with everything else. This assemblage was referred to as “bunk beds”, lending the name to this glorious undertaking. In one work afternoon we planned to remove the old bed and at least inspect/plan for new bed install. It was known to not be a drop-on installation, at least not with our knowledge of the light truck universe. That is, someone who has worked with Ford products for years could probably have identified a shortcut or workaround by reading on… well too late, we already did it the stupidest possible way! Actual installation was to be another day, with a week in between (where people had real jobs to attend to) where I would pregame making the needed brackets and assembling hoisting tools.

Removing the F350 bed from the stack was a 4-person job that involved sliding it backwards off the old bed and standing it upright on a large sheet of cardboard. It was then slid out of the way on the cardboard. I’d estimate it weight around 300-350 pounds – we could all handle it, but not with much finesse and certainly not for long.

So here we go! The first task in removal was identifying and removing all of the bolts holding the old bed on. The rusted-in-place carriage bolts with nuts underneath hidden by fuel tanks, crossmembers, and suspension components.

Half of the 12 carriage bolts were simply cut off at the heads because well, am I gonna reuse this? No. and the other half came off with differing amounts of effort.

This adventure took up a full half of the afternoon alone, and made me swear off the use of any independent nuts in the new mounting scheme. I’d much rather tighten bolts into threads that are machined into or welded onto (via weld nuts or tapped spacers/plates) the new bed mounting cross-members, than ever deal with a rusty Ny-lock nut again.

 

Lacking any sort of crane or hoist, we improvised with shoulder-slung steel tubes. This worked okay and clearly let all of us see who was the manliest man to ever man. Hint: wasn’t me.

This custom bed probably weighs north of 400 pounds (and is enormous) and while we were able to remove it, it was not with any precision. We basically dragged it off over the wheels.

This cannot be the case for the new bed, because it would mean a lot of damage to the underside. It’s built with more heavy steel than the F350 bed; we all thought it would weigh less, but in my opinion it was actually substantially more. Probably because it was designed from the start as a 5th-wheel mounting point.

And here it is, I now have a Vant. We just removed the -ruck part. There’s a lot of interesting and absolutely terrific things going on under that bed. First thing to note is it’s all mounted to 10 rubber body-mount bushings, not directly attached to the frame in any way. I don’t know if that’s normal for truck beds in general.

 

These are what I call “Precision Van Spacers”. They were under every crossmember, in varying amounts. I don’t know if these were “factory” or if someone installed them “aftermarket”. A good laugh was had by all.

 

What made me wonder even more was this large 5th-wheel hitch mounting plate. While it had Precision Van Spacer mounts in the end crossmembers, it was also welded to the frame through the angle brackets, here seen cut through with a grinder. So was the bed floating or not!? Anyways, this contraption had to be totally removed. It looks like it was supposed to be bolted through drilled frame holes, but someone made some interesting van decisions. I’l likely grind the remaining tabs more flush later.

I took the bushings off and….. I should not have taken the bushings off.

I didn’t need to see this. 1980s mulleted chain-smoker Charles would not have bought one of these now that he has had a good look at the build quality and, umm, craftsmanship.

So that’s the conclusion to Day 1 / Week 1. I now had to measure out and plot how to make new crossmembers to take advantage of the existing ragged Glory Holes torch-cut into the frame. <:(

I knew what I wanted was all topside service (no one guy above the bed, another underside, with some combo of breaker bars and push-me-pull-you dances) and no nuts. The new crossmembers would be fewer in number, as the F350 bed only has 3 rows of mounting holes, and likely just a flat slab of thick steel so I can thread into it directly.

Hey, look what’s easy to reach now! I replaced the rear fuel pump assembly and gauged the condition of the tank. Verdict? The rear tank is in much better shape than the front. This means the front tank had been out of service potentially for a year or two, if not more, gauging from its interior condition and the state of the remnant gasoline I pulled out. The rear would have been in use and cycling fuel through, preventing a lot of corrosion. The rear fuel pump wasn’t bad either, but the fuel gauge resistor strip had worn through (that’s why it didn’t read properly).

In the intervening week, I decided to just buy a Harbor Freight engine crane. I’ve had reasons to want one before, but never pressing ones such as “The landlords are asking why I have truck parts strewn about all over the parking lot”. As I mentioned above, we were not going to be able to wrestle the new bed on with any degree of precision, at least not with the GAINZ we’d be able to pick up in only a week, so a hoisting device was needed to take the weight while we did maneuvering only.

I also researched how people manipulate truck beds. This video (mute the soundtrack -_- ) ended up being my example, since he used the Harbor Freight engine crane. I’ve also seen two-crane dances and gantry cranes; while I would love to have a portable gantry crane, it’s basically a rigging job to buy one on its own and I decided it was beyond scope for the time being.

There was only one problem. The 2-ton Harbor Freight crane wouldn’t have reached far enough into the bed to balance it, since the truck in that video has a short bed (6 foot) and I have a long bed (8 foot). We thought about a few ways to counterbalance it, but ultimately I decided on doing it My Way.

This is #OSHAcrane:

Look away, Harbor Freight lawyers.

That’s an extra-long piece of 2″ square, 1/4″-wall steel tubing I drilled and machined to accept the same mounting hardware in order to make an extended reach crane boom.  Not shown is a steel biscuit that fits under it to take up the height difference between the outer tube and new boom. Otherwise it would have tilted down significantly and stressed the outer tube a lot more.

In terms of dimensions, the Harbor Freight crane is made with metric (C H I NA ) steel tube as far as I can tell. The inner adjustable boom measured 2 3/8″, or right around 60mm. I couldn’t get 2.25″ tube locally in time, so opted for thick-wall 2″ tube. If I wanted to make this again more correctly (…) I’d try to order metric steel tube online.

#OSHAcrane has about 18″ more reach than the stock crane. Shown under it is the two steel slats I’ll be making the new crossmembers from! They’re 8″ wide, 42″ long, and 1/2″ thick.

They are not light. But neither is VANTRUCK an aircraft or drone* and it really does need more weight over the rear axle anyhow.

*yet.

I arrived upon this dimension of steel plate by measuring and laying out the known mounting dimensions of the van frame and truck bed. I then picked two sets of body bushings which were the closest, and basically wrapped a rectangle around them.

The rear set of bushings would need to be moved up a few inches to accommodate, but I found that 8″ wide steel bar was sufficient. Otherwise, if I chose to not move the rear set, I’d need a 12″ wide slab.

Good thing I just got a milling machine running, huh? Bridget proved to be indespensible. I’d hate to have done this with a drill press, also inb4 get a plasma cutter. how about no

 

This is a finished replacement crossmember. The big hole is 3/4″ to clear a 1/2″ bolt with Van Precision – these get installed and tightened into the body bushings first. Then the bed is dropped on top and bolted from the top into the 1/2″-13 threaded holes.

Here they are installed! I had to machine out a portion of the forward crossmember to fit over the fuel pump.

Now it’s Saturday again, and we are once again gathered to shift heavy steel things a few inches at a time until Charles is satisfied. The rigging begins in the same fashion that the Ford Lightning bed removal video showed, using 4 ratchet straps, one to each corner of the bed. You can see that #OSHAcrane reaches exactly to the middle of the bed as designed!

” DESIGNED “. I make myself sound so serious.

This worked extremely well. The bed was raised just enough to move around…

…and up and over it goes! Flawless. We did exactly what we set out to do – provide guidance force only, and hold hoses and wires out of the way.

A snag – the shock absorber towers in the rear line up with one of the stock F350 bed crossmembers exactly. Well give me a carbon fiber enema…… why don’t I just mount the bed to those?

A half-hour of awkward step-drilling was needed to buy it some clearance. I drilled a sufficiently large hole such that the shock studs fall into them on each side.

Next snag! Ford, you assholes.

The rear set of mounting holes? 34″ apart, not 35″.  It was high enough up that I had a hard time getting a good visual alignment of the tape measure, and ended up making Certain Assumptions that “oh maybe they did a logical thing and made them the same so it’s easy”

Back to the mill I go….

After that fight was settled, the bolts were tightened down, and IT’S DONE! HOLY CRAP IT’S IN ONE PIECE AND IT RUNS AGAIN!

Here it is from the side. And you know what? i hate it.

Okay, not really, but now I am really thinking about a revision.

As we were drilling the two new holes for the rear crossmember, the thought suddenly occured to me that…. you know what, what if I just drilled new holes where they’re supposed to be, aligned with the truck bed crossmembers, so I didn’t have to use such wide steel slats?  I didn’t know how hard it would be to drill new holes (surprise: truck frames aren’t made of AR500 or anything, a step drill works too) so opted for the safe and quick solution of wrapping a rectangle around it. I was out to quickly get it back in one piece to not piss off the neighbors, over anything else, optimal solution be damned.

Second of all, I didn’t have a good way of determining the alignment vertically – the van frame curves up and down and was hard for me to get a datum off, especially in a beat up and unlevel parking lot. So this first pass at mounting it let me see what needs to move where.

I’d like the front edge of the bed to come upwards about 1″, and the whole thing should move forward about 1/2″ to close the epic cab-to-bed gap. I designed in the gap as a safety measure – would rather have too far than interfering – and now I’ve had a chance to see how it actually goes together, I can move them inwards for a more factory look…. not that the body lines meet or anything.

So there will be a Second Battle of Bunk Bed Hill. Especially that I know it’s super easy to lift the bed off with #OSHAcrane! I wouldn’t even need to lift everything, just one side at a time. I’m plotting the new crossmembers as 1.5″ x 3″ or 4″, 0.188 wall rectangular tube, and the new rear as 1/2″ thick x 3″ or 4″ wide steel strip. The tube would have machined 1/2″-13 coupling nuts welded through it to act as a tube boss (so the bolt isn’t just pulling on one wall of the tube) and the rear strip would be similar in construction to the current one.

With a significant source of stress lifted (heh) off my life by #OSHAcrane, I could now sleep easier and start picking at some of the smaller tasks. For instance, hooking up the new bed’s taillights. This first required some van spaghetti untangling:

Here’s all the factory, aftermarket, and after-aftermarket wiring extracted from the old bed. The F350 bed has all the lights terminating in a single connector, which is nice.

What’s not nice is not being about to find or source the matching connector. So I decided to improv and pulled out a 7-pin military surplus Amphenol connector from MITERS. Now I have even more America on this thing! Military-grade hardware!

Decoding the Ford connector was easy with a multimeter (and battery + suicide cable to see the lights turn on and off). All it then took was cutting off all of the van spaghetti and reaching back into the frame to grab the OEM wire harness and pulling it out. Here’s the terminated non-spaghetti lighting harness mated to the new bed.

The little green wire is a detail for later. That is supposed to be connected to the brake pedal switch directly, apparently so it can power a CHMSL. Vantruck does not have one, and I currently have no plans to install one (though if it will help keep texting idiots off my new bed…..) so I wrapped up this pin in the bundle for now.

All of the extraneous spaghetti removed, along with what sockets and bulbs I could salvage.

 

Something something about being lit, fam (shoot. me. now.)

The last major mechanical task is mounting the new step bumper, which has to be mounted on a long extension bracket to clear the bed. The Ford E-series step bumpers I bought do not have a cutout on the corners to fit around the bed like the F-series bumpers do, so I have to mount well behind the bed. I’m talking like a 8″+ extension bracket. This will be performed after I make adjustments to the bed position.

I will probably take a short break from Vantruck work, since it fundamentally is back in one piece, runs well, and is street legal lighting and fenders-wise.  At the least it can get out of its own way. Look for more work on Brushless Rage coming soon, because I want to push that damn thing to beta and to release this summer.

Operation ENDURING BROWN: Well, This Smells Familiar

Work on the beleaguered U.S.S. BROWN C. STENNIS has been continuing at a rapid pace! For what really is the first time with one of my projects, I called for extensive backup from friends willing to lend some elbow grease. First, because some of them are more “car people” than me, and second, because everything on this thing is heavy. It’s like the Chevy of trucks: cheap and heavy.

Wait…. Hang on.

This post recaps all the events of about 2 weeks ago following its return from my mechanic; I elected to take it back since it had not yet been consistently diagnosable (i.e. it was becoming a “throw parts at it” situation) and I didn’t want to keep running up labor charges. I ended up going through a series of cross-checks and inspections and discovered the problem was all too familiar, but obfuscated by a compounding issue. In the end, it was literally entirely my fault, so I’m very satisfied; unlike most people, I’m only happy if I caused the entire mess in the first place.

Let’s begin.

Prodding Ford Truck Bro forums and groups led a lot of Internet mechanics to suspect an ignition problem. The ignition coil on these things is tucked snugly into the valley between the two V8 cylinder banks (seen above) and its electronic control module can also succumb to temperature-related failure. As I described it, where the engine will start and run for only 10-20 minutes, it sounded like a temperature-dependent electrical issue.

I had my doubts, because it would only some times start and run for 10-20 minutes, and other times have a hard time starting at all. But seeing as these parts were all fairly cheap, I decided to outright replace them just in case.

 

That’s the Ur-ECU ignition control module. I like how it’s just bolted into the wheelwell stamping like a good ol’ retrofit system that got put into production. “Looks good here! Build ’em like this!”

So this didn’t resolve anything. I started wondering about other electrical systems in the path of the fuel pumps. For some reason, there are a whole bunch, as illustrated by this handy diagram I drew in a fit of frustration:

I managed to locate and test the fuel pump cutoff relay but couldn’t find any trace of the fuel tank selector relay. Based on some more sleuthing, I deduced that the DPDT selector switch might have been wired directly to the fuel pumps. The object that says “NEW!!!!” all over it is this contraption:

Another one of those “Well why the hell did you do that?” parts on this thing is the fuel tank selector valve. It’s basically a small hydraulic solenoid valve that connects one circuit to two, but shittier and plastic. And it was the source of one of my troubles.

See, while bypassing the fuel pump power safety cutoffs, I did numerous impromptu fuel pump volume tests (because I wanted to see if it was pumping fuel with shortcut wiring). This led me to discover that some times, the fuel volume was low or nearly nonexistent. It would start off good, and then taper off. This actually corroborated a weird behavior I noticed where some times when the engine would start sputtering, I would wiggle the selector switch repeatedly for a few seconds and it would gain some run time. This was in fact one of the symptoms that made me think a power supply to the fuel pump problem.

Uh oh. Suspecting that this valve had been bad from the beginning despite me testing it on the bench  listening to it turn over, I performed another volume test upstream of the valve. Both pumps were giving the correct volume, so I scrambled back to Pep Boys and picked up a new valve and spliced it in. I don’t know exactly what kind of failure mode it is – maybe the mechanism inside is sufficiently worn or damaged such that it might travel fine, but can easily be pushed out of position by fuel pressure. Maybe that causes it to backflow into the un-powered tank, or maybe it just plugs up and sits there.

The recurring lesson I’ve been learning from VANTRUCK is “BTDMIW” :  But That Doesn’t Mean It Works. Just because I jiggled the component on the bench, or in isolation, doesn’t mean it actually is working correctly when installed.

But there was more! The fuel being pumped from the front tank, the one I personally serviced with a new pump and float  – was rather BROWN. It was darker than what I usually knew gasoline as. Even more telling was that there was sediment on the bottom of the jar.

I instantly knew what was happening. The next thing I did was run around to the front and start unscrewing the carburetor fuel inlet line:

…and I sheared it off in the process, because I untwisted the first big nut looking thing I saw, but it was really the nut that went into that nut. Brilliant!

I couldn’t even blow through that little metal sponge. It’s the “filter of last resort” for the carburetor, and it had trapped in it all of the rust slurry being pumped from the front tank. You can see some of the visible grunge on top.

Dedicated readers might recall that I also replumbed the fuel tanks in the same operation that I replaced the front fuel pump in. Even more dedicated (or observant) readers will also notice that I did not install an inline fuel filter on the front tank. Why? Who knows?! Maybe I’m just traumatized by fuel filters. Maybe I thought the fuel pump’s jizz sock thing was enough.

I patched this section of steel fuel line with some rubber hose and called it good.

Here it is installed behind the zinc-chrome part in the lower center. That is a “vapor separator valve”, or as I kept calling it, the vaping valve. It was bypassed earlier this photo series by a chunk of fuel hose. Unlike a modern fuel injection system where there’s a fuel pressure regulator bleeding off fuel into the return line, this is just a little pipe with a hole in it. Its nominal purpose is to prevent vapor lock by having fuel vapor escape through the little hole, along with small amount of fuel. Ford sells these in several hole sizes depending on how much you want your engine to vape and also to help modulate fuel pressure. What the hell? Almost every system on this vehicle in some way is analogous to touching a variable resistor to something. None of this is okay.

And you know what? It ran GREAT!  Rev for days! Piss of the neighbors!  A M E R I C A N  P R I D E. Oh crap, what’s that smell??

This is a giant puddle of BROWN  that was slowly increasing in magnitude as I was having too much fun firing gun-wielding Bald Eagles out of the exhaust. Which, by the way, was backfiring (afterfiring) like crazy. It was clear the thing was running super rich. I now had literally the opposite problem as before. Hurray!

A little research showed that all of this BROWN was coming out of the vapor canisters. So much fuel was getting into the carburetor that it was coming out of, and flushing, the vapor collector lines and washing out the canister. Great! It’s like clearing your sinuses!

(The parking lot is still BROWN and smells like a freshly coated gym floor there, to this day)

So what was the cause? I dug into the carburetor manual a little after observing it with the air cleaner removed. That’s where I discovered another “tighten the incorrect nut” problem.

I found a little nut on the carburetor that I thought was left loose by the mechanic; since, you know, I kind of bailed it out of their hands before they could put it back together. So I tightened it. All the way.

Well it turns out that’s the fuel level adjust screw and accompanying locking nut for the secondary throttle (which only opens after about 50% throttle travel or so). All the way down is all the fuel, all the time, forever and ever. I noticed the secondary throttle discharge was completely wet even while idling.

This screw was adjusted more correctly.

 

And off we go! I went on a “Lap of I-95” test. On the whole, performance was excellent. I made a point to exit and then re-enter the freeway repeatedly to do full throttle pulls from ~25 to 70mph. It still tended to be a little backfire-y when letting off from high throttle demands. Given that the mechanic didn’t have a chance to properly tune and road test, I think something’s still a little whacky, but that is now an addressable problem.

Hello, Mr. Tesla. Get in my belly.

In the end, I concluded that there had to be a very specific series of events and misjudgements for the running condition to get this bad. Here is my assessment of what happened:

  • I replace the front fuel pump. Given that I had no lift and was working entirely on the ground without help, mostly in the dark, I didn’t drop the fuel tank fully and inspect it. I only lowered it enough on the straps to grab the fuel pump. Therefore, I didn’t see how much rust was inside.
  • When the front fuel pump went back in, I neglected to install an inline filter on the output side.
  • Filling of the fuel tank with new fuel, plus the force of the collision, likely washed a lot of loose debris into circulation, where it was picked up by the pump.
  • I specifically used the front tank around town and during the Motorama trip attempt to ensure the system was operational.
  • The carburetor began clogging with this rust slurry, causing me to abandon the Motorama trip as problems gently surfaced.
  • Gradually, with additional around-the-town usage, it became worse as more rust slurry blocked the caburetor inlet screen.
  • The particulate debris MAY have also affected the operation of the fuel tank selector valve – I am uncertain if it played a substantial role in the earlier problems.
  • The mechanic was able to test for proper fuel volume delivery because the valve problem was a some times thing, which incorrectly ruled out the fuel system as a source of trouble. The Ford official player’s guide makes you only time the delivery of 1 pint of fuel as the test. I was pumping into a 5-gallon gas can and was purposefully holding the pumps on for a while in case something caused them to lose power.
  • After the carburetor rebuild, I told him to continue testing using the front tank, because the rear tank was in an unknown state to me and had a non-functional fuel gauge sensor, whereas I said I had replaced the front fuel pump and fuel gauge sensor.
  • Furthermore, for debugging systems in isolation, they bypassed the fuel tank selector valve completely and directly piped the front fuel tank to the carburetor.
  • The carburetor began clogging with rust slurry again, leading to much the same symptoms and to the frustration of all involved.
  • This timed well with me electing to cut my expenses and asking them to stop work.

So there you have it. Once again, one of my vans is stymied by the uncertain nature of fuel delivery. You know what? Electrons don’t need fuel filters! What are you gonna catch, some neutrinos?

How bad is the front tank? Probably very. Before I turned anything on again post inspection, I went and bought the biggest clear inline filter Pep Boys had to sell and dropped it on the front fuel tank’s output line. That’s what it looked like afterwards. Delicious, delicious BROWN . I’m not likely to do any fancy fuel tank treatments to stop this. New replacements can be had for $100 or less, and as long as the bed has to come off, replacement will be easy. Plus, unlike Mikuvan’s filter, these two things are easy to reach, so I am likely just going to keep changing big plastic pubbles first and foremost.

Next time, the action starts for real: