What’s Inside that Surplus Center Bomb Hoist Motor? A Quick Break from BattleBots with Beyond Unboxing

Hey everybody! I’m back with a new episode of Beyond Unboxing focusing on a very unique piece of hardware that I just got way too curious about. In searching for a small American separately-excited (SepEx) motor, I remembered an item I saw on Surplus Center quite a while ago that they seemed to have a lot of trouble selling.

Huh. With no datasheet/manual/pinout available, the odd form factor, and shipping being extremely expensive due to it being heavy, I can see why I think they’ve only managed to sell 5? within the past year. To what other crazy dumbasses, I wondered. This motor definitely had at least 1 of the characteristics I was searching for – it was very American indeed, what with being American made for the American military to drop American bombs – and this will come into play later.

As for being sep-ex, I was at least very convinced it was a field-wound type motor, not permanent magnet. It seemed juuuuuust old enough that permanent magnets wouldn’t have been cheap in that size and not offered as much performance as a big series field winding in the required application – winching something. The multi-pin wiring harness coming out of the motor also indicated a wound-field type to me, since I couldn’t imagine this motor having an encoder or temperature sensor. Perhaps 2 of the pins were a load-holding brake, since hoist and all. But that still left at least three pins!

Not even mentioning the odd lobular shape of that gearbox of course – that got me even curious-er about what went on inside. Just looking at the thing, I counted at least 3 stages of gearing mentally, and with the weight of the whole assembly, there must be some seriously massive gears inside! So I went ahead and purchased one, just one, for merely 40% of the final checkout price as shipping this object was $75 alone. This better be really good…

Aand I’m glad to say that it WAS VERY GOOD INDEED, a journey into a vestige of the big & brute force style of American manufacturing where the product is an engineering textbook in physical form, and containing quite a few pleasant surprises. MURICA ONWARDS! Also, I managed to trace out the wiring for the motor, so there’s that.

First of all – They’re serious. It’s heavy. There was an attempt at shipping it correctly, for sure – the thing was firmly pallet-wrapped to a piece of thick particleboard on the inside of the box which had kinda survived transit. There were several holes punctured in the box also.

I wasn’t worried for it at all, obviously. I was worried more for what it took out on the way down the conveyor, like borderline expecting to pick the debris of someone elses’ Amazon sex toy order out of the motor fan grille level of worried. Luckily, my fears ended up unfounded.

It took… some effort to get this damn thing on the table. That’s an 18″ (0.5m) ruler next to it… the whole assembly is over 2ft long end to end. That’s a lot of little safety wire too, all neatly wound and tied off.

The motor has a nameplate on it showing it was made by the Steel Products Engineerng Division of the Kelsey-Hayes Wheel Company. Looking up the latter, I saw that they did indeed make many wheels, among other things – certainly during any of the 20th century war efforts they would have made military gear.

I back-searched the order number found on the motor and gearbox plate AF33(602)7109 and found some listings for a canceled defense specification from 1982 – so this would probably imply the units were manufactured well before then. Searching out that Mil-Spec MIL-H-25205A(1) showed that it was published as early as 1960. And searching the NSN (NATO Stock Number) 1730-203-8712, in the form of 1730-00-203-8712 yielded a 1963 date. So it could mean these things were built around the Vietnam War era.

Most of the info I could find was buried behind spammy paywall websites that aggregated mil-spec info. I wasn’t in the mood to research out the history of this damned thing, just to take it apart and see if I could use it for unintended purposes. I’m guessing after these were all decommissioned, they got stuffed in a warehouse in some recently-closed Air Force base before making it onto the surplus markets. Anybody who has more information on these, or if you’ve used one in real life, is welcome to tell me more about them! Would you recommend them to a friend?

The nameplate on the gearbox housing yields about the same information.  Based on my understanding from some light research, these were hitched to planes to lift bombs into position, but the planes did not carry them along for the ride. The numerous quick-release features and handles on it do imply this object was intended to be quickly moved in and out of position. I’m guessing the whole operation looked kind of like this, but I must balk at the unwieldiness of this device for such a purpose. Maybe 75 pounds is only heavy to me.

It is quite adjustable, however. The unpainted aluminum casting at the front pivots if you pull a pin, and can lock into one of six positions. The base has a pullable locking pin also, as well as four riveted shouldered sliders (two rivets visible above) so it was definitely designed to slide into something and lock in, then be removed quick.y

 

It also comes with accompanying toys – the tackle block and its accompanying 8-tooth ball-bearing-mounted #80 hard chrome plated sprocket, and its mating friend, an extendable wrench which fits into a cavity in the sprocket for when you need to give your bombs some manual assist. The fact that a #80 chain is the preferred hoisting medium still boggles me.

Let’s start taking this thing apart! First, there’s a spanner nut that retains the quick-release assembly which needs to be unscrewed. Absent the correct tool, I just used a needle-nose plier. The quick-release assembly has a 7-tooth #80 sprocket inside which has a splined bore for being driven by the gearbox.

There’s the drive sprocket. The chain enters through the vaguely H-shaped guide slot in the bottom of the quick release, and is fed into the sprocket and kept from losing contact by guides (and probably by virtue of being huge).

There’s a rotating cover of some sort which is retained by a pin – once the pin is driven out, the cover is removed and the sprocket is no longer being detained and is free to leave, thank you very much. Now you have a 7-tooth #80 sprocket to play with that fits on that specific type of splined shaft, which will be removed in due time!

I continued removing all the ‘jiggly things’ so they wouldn’t get in the way later. It has some other small clips and handles that all are held in by mildly press-fit pins.

Oh, and safety wire. Did I already mention all the safety wire? Everything is safety wire.  In beginning to remove the motor for my appraisal, I had to spend 5 minutes cutting and extracting all of the safety-wired screw heads!  I noticed the screws themselves were barely tight for the most part, with their only saving grace being safety wire. I assume this is not actually standard practice in the aviation industry…

All of the bolts are US threaded – they are generally 5/16″ thread, using a 1/2″ hex drive. Here we go! About to crack the motor off…

And let there be PEANUT BUTTER. There is a heavy grease packing inside which can only be described as peanut butter – it’s everywhere, and it smells straight up pre-EPA carcinogenic. You know that “Old Electrical Equipment Funk”? It’s that, but on anything it touches. I ended up digging a lot of it out with shop towels later and throwing it ot…. but part of me regrets it now and wants to keep the grease of the next one(s) I buy (if I do) in its own little jar for future generations to appreciate.

But here we see where I have already made wrong assumptions about this thing. I assumed it was a direct drive off the motor into the worm gearbox, or at most 1 stage of gearing. However, looking inside at this point, I see at least three stages of spur gears.  It’s interesting to note that I haven’t found a single molded plastic part yet – everything is rubber, phenolic, or metal.

Here is the motor by itself. I’m going to dig into this thing a little in order to find the pinout of the 5-pin circular military style connector, in the process discovering the type of winding it has – whether it’s series or shunt wound, or a seperately excited motor like I want.

First, four tiny safety wired!!!! screws need to be removed for the rear cover to pop off, which only houses a fan.

You may be wondering what that little “Westin Elevator Shaft” contraption is on the side. It’s a captive hex shaft which has a socket on the other end that mates to a hex stub in the spur stage of the gearbox. It seems like its purpose is to allow hand-cranking of the gearbox through the reduction the motor sees – presumably while your buddy is standing on the end of the manual tackle block tool also, so you can hoist bombs even when the power is out.

Another set of SAFETY WIRED!!! tiny screws and a shroud that covers the brushes is released. This doesn’t affect the brush holder – it only allows you to see into the ventilation holes. I’m guessing this motor might come in several flavors including open (like this) or enclosed/fan cooled (like it was before I cracked it open) depending on options.

The fan is retained by a single nut, and removing it exposes the part of the motor which I suspect was designed last.  So here’s what’s going on:

  • The outer ring of 4 nuts hold the whole endcap onto the tie rods that run the length of the motor. These are structural to the motor. They’re #10 thread, so a 3/8″ hex drive, except one by the Westin Elevator Shaft which is a “thin pattern” hex nut using a 9/32″ hex drive, probably since there isn’t enough space for a bigger nut.
  • The inner ring of 4 nuts retain the brush holder onto the endcap, and are #8-32 nuts, so a 11/32″ hex drive.

So there you go: 3 tools to do this operation, all within a few 32nds of each other. I was confused as hell about what was just painted over or not and if i was really seeing things or there were #8s and #10s in close proximity. ‘Murica

 

While I was undoing the endcap, I also unfastened the giant die-cast junction box and unscrewed the circular connector to try and find out if there were obvious armature/field wires. They all disappear into the motorial abyss, so I’d need to keep exploring.

Continuing with the theme of “no plastic anywhere”, all of the wire in this thing has braided insulation!

So I’m a wee bit confused on the order of operations needed to assemble this thing. I clearly did it the wrong way, which is to remove all of the endcap nuts at once and yank. The inner ring of nuts retains the brush holder and also locks it in a certain brush timing, which I will not be able to recover exactly.

What I think is the correct way to disassemble the motor appears to be removing the tie rod nuts (outer ring of nuts) and then removing both the armature and the brush/endcap assembly at the same time. That way, the brush holder isn’t disturbed, and since it’s a wound-field motor, you’re also not fighting magnetism to do so. Something to keep in mind for next time! I’ll show how to disengage the armature in a minute.

This brush setup is quite something. The brushes themselves are circular arc shaped and they pivot on little arms, instead of the traditional inline coil spring setup. Wonder why they did it this way? You potentially get more brush life from the small amount of space the other springing methods would take up, I suppose.

To pop the armature out, use a thin 1/16″ pin punch to drive the pin out of the pinion side. The pinion, it turns out, lives on another spline and the pin’s only for axial placement.

Then you yank. That’s a real pretty armature – it’s wound almost like a starter motor (which I suppose it will share a lot of intermittent-duty high-power lineage with).

Of note, it has a large flat steel faceplate. This is related to the next photo:

First of all, field windings and brush terminations! This allowed me to back-trace much of the 5-pin connector. I determined that the motor was indeed a separately-excited (Sepex) motor!

You see the fibery-looking pad at the bottom? That’s a phenolic brake pad. It’s spring loaded upwards naturally, and you pull the little pin on the right to engage/disengage it. It mates with the steel disc that is on the armature. When it’s engaged, the motor shaft is hard but not impossible to turn. It’s likely a load-holding brake for the motor and is there more as an extra precaution – unless that worm gear stage is very high helix angle, I can’t imagine the motor contributing all that much to load-holding versus the worm gear.

Repeat after me: “Reassembly is the opposite of disassembly.” I discovered that my “correct way” of disassembling the motor was in fact not going to be possible – there’s two attachments to the brush holder that are screw-in and must be obviously done so while the brush holder is not mounted to the endcap!

So the way I did this reassembly was armature, then brush holder, then the two screw connections, and then the endcap (then thereafter the fan shroud and so no). As for how the factory made sure the brush timing is correct…. hell if I know. I did my best by visually inspecting it through the vent holes.

You know what? Just don’t take the motor apart and take my word for it.

Since the motor was really my agenda, I decided to do some basic characterization of the motor. For my sepex application, I would like to know the field resistance, armature resistance, and ideally the magnetization curves of the motor – no-load voltage (out) versus field current for several different input speeds.

The problem was I would have needed a controlled way to spin the motor up to around 10,000 RPM, so I didn’t get any of the magnetization curve data for the time being. I found out that on its native stated specifications – 28 volts applied to both field and armature – it wanted to draw 6 amps spinning no-load at 9,200 RPM. For such a big motor, 9,200 is really fast…. but the 8,000 RPM @ 44A specification on Surplus Center made more sense.

I also solved the armature resistance to be 0.04 ohms and the field resistance to be 10.1 ohms. This is one hell of a motor – albeit only for a short period of time, which sounds perfect.

all together now… what the fuck is he building now that needs this specific motor? doesn’t he design motors for fun?

To summarize this section for now – here’s a pic of the circular connector showing the pinouts I discovered.

That ought to fix all the buyer questions on the Surplus Center website, and hopefully make this thing a little more useful if you have a #80 chain hanging around that needs something to climb up it slowly.

But the story doesn’t end there. Oh, it’s just beginning. There was still 30 or so pounds of gear that I haven’t even opened up yet.

I’ve already found that my assumptions about the input stage were wrong. What ELSE don’t I know about this? Let’s remove the 25 miles of safety wire that hold the back gearbox cover plates on.

I actually decided to work forwards from the motor and start on removing the worm gear stage first, since I got very curious about what kind of worm gear it was which they’d still warrant a load-holding system on the motor in the form of the spring-loaded brake. The six inner screws release a cover plate for the bearing of the worm wheel axle. The outer six safety-wired screws hold the entire endcap on; it’s a mild press fit, so be prepared with a sharp paint scraper or knife edge to do the initial release.

The worm gear system is now exposed, but it’s not yet removable since it doesn’t have enough slop in it to wiggle past the wheel past the worm.

The other side of the worm wheel axle is just the large back-side cover. Time to take all those screws out and start paint-scrapering to release the press/grease fit!

First off: Holy crap, that’s a lot of peanut butter. Second: Holy crap, that’s another entire intermediate stage I wasn’t expecting! Third: Holy crap, those gears have stub-form teeth! I’ve only read about that in engineering textbooks of my bunny days – never seen stub gears in real life before.

Once this back cover pulls out, by the way, the worm wheel just falls out the endcap side (bottom in this photo).

The worm wheel is kept in place by the compression provided by the spanner nut, but power is taken through an involute-splined hub. Notice the small gear stage next to it. This is a mere 1.25:1. The gear at the bottom of the worm wheel axle is 12 tooth and mates with a 16/12 tooth cluster gear which does the final mate with the large output gear. I must wonder what type of packaging concern or ratio fine-tuning warranted this intermediate stage when you theoretically could have tuned the worm gear or output gear one way or the other slightly.

The worm stage is a double-enveloping type, also called a globoid worm design, for maximum strength and contact area. This thing has just been an engineering textbook in a peanut-butter filled box so far; it was actually quite pleasant to see again, given my recent forays into electronics and shitty vans.

I sprinkled the final drive out of the casing, only to discover….. more peanut butter. Go figure.

What was also cool to see: Inch-sized big-bore thin section bearings. These days, the dominant bearing is the metric single-row series (6002, 6200, 6801, etc.), but there is not a breath of metric on any of this. The bearings all were crunchy – unsure if it’s due to aged and dried lubrication or just specified to be a lower uniformity/finish grade, but I’m going to yank them all off and keep them.

After I cleaned the peanut butter off for the most part, here’s the final drive. The output shaft isn’t actually retained by anything but the back plate – once it comes off, the shaft will fall out. It also isn’t carried on its own bearing, depending on the distal bearing found in the aluminum mounting assembly with the swivels that I removed first. So the green gearbox wasn’t ever supposed to live on its own either.

There was still a worm gear stuck inside and the 3? stages of initial spur gearing I haven’t discovered yet, so back to the other end we go! The same procedure is used on the motor side: cut off all the safety wire and just start unscrewing. This side has some dowel pin alignment mates which are more press-fit than the rest.

Aaaaaaaand more peanut butter. By this point, I’ve almost half-filled a 44-gallon rolling trash bin with towels full of peanut butter stains.

The setup didn’t make any sense to me, as I was clearly spinning the motor pinion’s mating gear by hand but seeing two different rotation speeds. In fact, the hex shaft which couples through motor into the (missing) manual crank handle is geared up from the handle itself, but at a different ratio to the motor which is geared down in two stages. They put a complete independent gear path in here just so you can spin it by hand – I’d like to think it was informed by how much torque it was comfortable to keep applying versus how quickly your arms get tired from cranking.

But it was probably because steel was basically free back then.

After another container truck left for the JIF factory, we expose the final boss of this gearbox: the screw holding the input gear on.

Actually, no. It was in fact easy to remove that screw, but hard to remove the two gears in front of the worm input gear. They’re just press-fits with bearings ,which I had to “three phase screwdriver” pry the upper right (motor input) gear out, and slide hammer the hex shaft gear out (attempt 1 with a vise grip is shown…. attempt 2 is hooking my slide hammer onto this vise grip) trashing the tiny inch sized angular-contact bearings in the process.

 

F :(

 

The input pre-duction has been freed!

….and there are more screws. And more safety wire. 2 health bars? Nope, this thing’s had like 20 extra lives by now.

After that gets undone, the worm gear pops right out! Hurray!

Here’s the final gear count: Seven, each intricately engineered and machined, with polished teeth and edges. Go watch some worm gear machining videos and then talk to me about how sweet this thing is. I’m not sure how I can even use any of these gears outside of the box they came in, because I sure as hell am never going to make the worm gear fit correctly in anything again. The temptation of bringing Cold Arbor back, though, went up several-fold after doing this surgery.

So what’s the ratio from the motor to the big 7-tooth sprocket? The input stages are made of two stages of 54:14 (14 tooth pinion on the motor, a 54/14 cluster gear, and 54 tooth worm shaft input gear). The worm stage is 30:1. Then you have the 1.25″1 intermediate stage (12 teeth on worm shaft onto a 16/12 cluster) and finally the 36-tooth output gear. That’s a total of 1673:1 and some spare change.

I’m inclined to say that this device is really best kept together, maybe with your own assembly in place of the swivel mount, and using the motor as-is also; maybe doing some work to adapt the input shaft to your own motor.

There’s so much excess it’s a joy to behold: In its day, steel was free, labor was cheap, and China wasn’t a real place.

alright, so what the fuck are you building that needs this precise kind of motor, the more American the better?

All will be revealed in due time, but it’s exactly what you’d expect. I’d like to collect some magnetization data on the motor soon, so I’ll report back in with its operating characteristics at several voltages and speeds. I’ll likely end up purchasing another one GREAT, MORE PEANUT BUTTER and making a face-to-face dynamometer to collect said data (maybe not full dyno curves, but at least the bemf-versus-speed info) since the best way to characterize a motor is to drive it with itself, in an electrically masturbatory loop of power.  I’m thinking of how I’d incorporate the rest of the gear stages, but it seems unlikely with the ratios I can arrange them in. All I can really say since I don’t have a definite timeline due to my startup-baby, is that it will bring some interesting new-old tactics into a game with an established meta; it won’t win anything, but will be glorious while doing so!

The Overhaul Design and Build Series, Part 5: “Don’t you have to ship this on Wednesday, dude?”

Yes, yes I do. STOP REMINDING ME OR YOU’RE HELPING MACHINE THINGS.

Well here we are, after the airing of the Overhaul vs. Sawblaze fight which will be on Science Channel’s website and other streaming service soon! I have a full writeup I need to do on the lead-in and post-match analysis for that one! That will come after the conclusion of the build series in this post.

We rejoin our heroe…. dumbasses in the 2nd-into-3rd week of March. March 21st was the latest ship date available for east coast teams in order for everything to make it there on time (or so we were told!?). Luckily, Overhaul was actually not in a bad position, at least compared to Season 2 when the extra long days really started kicking in. All I really had to do at this point was a final assembly, then work on remaining spare assemblies.

After the Week of #WeldingGoneWild, it was actually very easy to do a fitting of the whole front of the bot.

That’s about it. The only thing which wasn’t added in this photo was the clamp actuator itself.

I’m much more a fan of this design already. Once the whole thing is loosely assembled, there is a degree of “elastic averaging” *ahem* that goes on as all the bolts get tightened down, but after that, the arms are rock solid.

The drivetrain is being assembled more now. Check out the Markforged nylon engine timing chain style guides! The front chain was still a bit loose after this so (at the event) I ended up making a different set, to be shown.

The one on the right between the two motors is a little ridiculous. We were running so tight on time that I wasn’t going to get the #35 half-links of chain in on time, or at least too close to risk not being able to drive test. So I invented the stupidest possible chain -pincher for the intermediate drive chain – it was gonna wear out very fast with its profile, but would at least let me get some test driving in.

Closing up the other drive side. The design for serviceability that I did 2 years ago is really coming back to help me here. Remember, my team this year is scattered – Paige is working a real job across the country, Cynthia is occupied full-time and could only help on a limited basis with set-up operations, and I only had Allen’s help briefly with welding too. Most of the photos taken in this build series was work done by myself solely.

Here’s the first test-fitment of the entire bot with all hardware installed. I’m really liking all the design changes to the steel parts. In person, the new clamp and forks look better proportioned to the bot. At least to me, way better than OH2 for 2016.

(Fun game: See how many dumb project artifacts you can spot in the background of this and other photos. Chibi-Mikuvan currently resides under my desk.)

 

I spent an evening just pounding out spare parts for the incipient shipment. For one, I was short on drive motors now, but with a shipment of new HobbyKing Sk3 6374-192s waiting, I needed to key the shafts and secure the hardware. It was easier to pop the shafts out en masse and set up the mill properly.

This and more! I went through….. zero 2mm endmills, somehow. Still a harrowing operation.

It was now the weekend before, and I realized that I wasn’t going to be able to get my last round of waterjet-cut parts in time. These days, I get to be in the back of the line for MIT shop waterjetting – which I think is a very reasonable voluntary position to be in, as I have no official involvement any more with the institute. But dangit Sawblaze, you guys still do!

The electrical deck could conceivably just be drilled from a plate of aluminum, so that is what I ended up having to do. Out comes the TERRORISM. I just cut a chunk of 1/4″ aluminum plate out and started marking holes like high school Charles would have done, and he is always right.

Please do not ever, ever, ever do this. This is how you die. This photo is for illustrative purposes only and should never be attempted, building a robot is dangerous, etc. If you do, use the finest tooth blade you can get and have someone else pump WD-40 or cutting fluid constantly. Or you will die.

 

In the middle of the process. All the small holes are #4-40 tapped for Brushless Rages. Notice how I put six holes in some positions? This will be important later.

 

I’m loading up the bot with electrical deck hardware and wiring now. The shock mounts are in (and secured from the bottom) and some of the battery harness is visible.

The wiring for Overhaul this time was…… ad hoc, to say the least. I said I would dispense with the carefully cultivated greenhouse of busbars. The fanout occurs at the master switch terminals this time, with 8 gauge main leads splitting into multiple 12-gauge intermediate cables to the Brushless Rages. Single 6-AWG conductors handle the “fan-in” from the 4 batteries to the master switches.

The octopus taking shape, with ESCs installed.

Remember those 6-hole patterns? I had to temporarily use the 6-FET models for drive, keeping the 12-FETs for lifting and clamping.

What, are they magic or something? In actuality far underrated from their published specs?!

No, but I accidentally sold my entire product line – which is great – leaving ME with no remaining 12-FET units – which isn’t great. I had to dig into all my pre-production units here to even complete Overhaul at all. What is stock tracking even??

I wasn’t running off a cliff without a drone backpack, by the way. A month earlier, I had placed the assembly order for a new batch of Brushless Rages, but they wouldn’t get in until the Monday of the ship week and I was not taking any chances.

With the octopus wired in, the drive base is live for the first time. Check out the motor-on-a-stick I used to simulate having a clamp motor.

 

Overhaul prior to its first indoor test drive! At this point, I’d fight in 20 minutes if I had to. I think I was actually ahead of the curve here by a distressing amount.

 

I cleaned up and routed more wires into loom in order to un-nest the wiring some. This is inconceivably ugly to me, like a steaming fresh pile of partly-regurgitated dog squeeze smeared across a sidewalk by multiple unassuming passerby. I would never ship this in a consulting project. Yet some of y’all at the event said this was the cleanest wiring in a bot ever? What the actual hell is wrong with you?

(After seeing inside everyone’s bots, I’m not inclined to disagree. Sorry not sorry.)

 

Monday came, and hey! Look what’s here! More Brushless RageBridge units for all! I’d end up assembling 25 12-FET units and packing them with me to the event (not including my own spares, which were 4x for drive plus another 4x for spare overhead)

One of the put-off things was welding the wedges together beyond just tacking, so I spent much of Tuesday doing this. The plan was to take the tacked units to MIT to use one of the MIG welders I have access to and really smash them out quickly.  Using the bot itself as a welding jig made for expedient alignment of all my wooden dinosaur puzzle pieces.

DETHPLOW ™ was tacked together in the same fashion, by actually mounting all the pieces to the bot and locally squeezing with clamps.

For completion purposes, I fully TIG welded one set of pointy-wedges and mounted them on the bot in their final positions. TIG welding is truly the wrong technique to use for bitey pointy robot parts, in my opinion, since it takes so much time compared to MIG in an application where the sensitivity is not really reflected in the end product.

As I mentioned previously, it ended up pissing us off so much we immediately bought a MIG welder after we all got back from the event.

This, for instance, is DETHPLOW all MIG-welded together, a process which took only 15 minutes or so once it was jigged up. I designed all these pieces to be MIG-filled anyway. Here I am doing some TIG touchup on areas which I fell a little short with the wirefeed or missed, or had a gap that I couldn’t bridge as the fitup wasn’t 100% perfect. This is a fine state of affairs for me – blitzing and then fine tuning if needed.

One thing which occurred over the weekend was crate setup. I decided to just spent money this time to get an elegant and reusable SINGLE. PALLET. solution. As someone who’s had two double-pallet crates wrecked over two BattleBots seasons for reasons unknown, I decided I was much better off with a tall single pallet. U-Line came to the rescue with this 4′ x 4′ x 6′ tall snap-together crate,which I modified by adding some removable side-in shelving levels. The bot with its lift table and large tool chests/boxes was to fill the bottom floor, and more containerized accessory suitcases in the middle, along with the pictured Markforged gear – Markforged went ahead and lent me a 2nd printer for the event.

The top level would contain the loose large parts such as the frame rails and spare welded assemblies.

You know all those spare-everythings I was cutting and machining? They ended up in a tote which contained all the important mechanical bits of the bot. I’d prepped a full set of drive and lift motor spares, along with a few mor prepared motors. There was also enough cut tube sections to weld up a new clamp at the event if it came to be.

 

And here it is, Overhaul and all of its support equipment and tools plus spare parts, all ready to load up into….

 

Vantruck??????????????

 

THE PLOT THICKENS! During the week prior to shipment, a few of us NE builders came together to ally ourselves against the forces of time.

You see, Team Forge & Farm was planning to road trip across the country with their bot in tow. For a nominal fee of a few spare RageBridges, they were willing to also bring Overhaul along.

This effectively bought me an extra 4 days to work on the bot – in fact, the electrical work and spare welding photos you see were done after the 21st. On the Monday following shipdate, I picked up HUGE along the way and ended up in southern New Jersey.

 

…where, under the cover of darkness, we packed Earl’s truck up with our bots and his alike.

So… what’s in the crate? Well, there was still the lift cart and all of the already-completed spares, the printer, the mechanical tote, and other support equipment like the battery chargers and power supplies, and a few doen Ragebridges of various flavors. I handed off the radio suitcase and both of my event toolboxes off with the robot.

 

There were still a few kibbles I had to take care of after the bot went out but before I did. So, how do you jig up pieces for welding with you don’t have a robot???

You 3D print an imitation of the robot! This is an Onyx print with the same hole spacings and offsets as an Overhaul front frame rail. I used it to tack the pieces together quickly (as to not melt anything) before removing them.

And with that, the build of Overhaul 2 for the new BattleBots concludes. To be entirely honest, I found this build season pretty stress-free, largely because I didn’t have to build a new bot from scratch and was making only well-scoped changes I had anticipated in advance. In the position I am in now working on a new company with my friends, I don’t think I could have pulled off the record build of OH2 for Season 2 in 2016. My (and my friends’) experiences in this build and competition season of BB – without going into NDA details of the show – has really shown me that I have to move back to a “When it’s ready” format like I had to do during my busiest times at MIT trying to vaguely graduate on time. I have a lot of thoughts on the show as a whole and the direction I’d like to move in (and the show should/shouldn’t move in) that are much better reserved until after the entire show airs.

But for now, hang out here a bit for the event report and a SawBlaze vs. Overhaul post-match!

And now a word from our sponsors!

HobbyKing – Somehow still loves me and enthusiastically supportive of my efforts to abuse R/C model parts for unintended applications! I’m running a HobbyKing radio (9XR Pro) and batteries (Graphene 6000 65C 6S packs, times 4), motors (SK3 63-series), BECs, and a whole lot of wiring and connectors. Not to mention the Reaktor battery chargers and who knows what other HK kibbles have made it into my tools and accessories. I like to think that I had a large role to play in the commoditization of silly electric vehicles using R/C parts also.

MarkForged – from the days when I knew 50% of the company to today when half the new marketing and sales staff go “Who is…. Professor Charles?”, they’ve provided me with high-strength printed parts for a lot of different projects, both on this site and off. Introducing them to the robot fighting community via Jamison’s and my efforts pretty much made MarkForged printed-unibodies the competitive standard in the 1 and 3lb classes, and trying to find new niches in the bigger weight classes is one of my goals. This time, Overhaul’s drive wheel hubs and casting molds are printed from Onyx, and there are also plenty of smaller chain glides and tensioners and accessory parts.

SSAB – I find it interesting that the company’s full name is SSAB AB – Svenskt Stål AB AB, or Swedish Steel Company Company, but these days the lettering is the whole company name so that’s actually not true. This year, I’m working with one of their North America regional distributors and all of the armor steel on Overhaul – including the entire clamp arm, top plates, and new wedgelets and DETHPLOW™ are Hardox 450. Hardox is the easily-obtained ARx00 of Europe and other regions worldwide, and bots overseas have used it for years, but it’s not really had a foothold here in our scene compared to the number of AR-spec steel products in the US. So hopefully I can help with advancing that brand too!

BaneBots – I was called an edgelord for even thinking about using P80 gearboxes in a modern Battlebot. I always thought they were under-loved after the FIRST Robotics Competition quality issues of the late noughties, and had used them otherwise in several projects including consulting projects before shoving shorty Ampflow motors into them for Overhaul 1 in 2015. And you know what!? They’re great! Overhaul 2 ran them exclusively for Season 2, and now for Season 3, OH is sporting the new BB220 series with much stronger planetary output stages for the lifter.

Equals Zero Designs – Yeah, umm, I don’t know much about those assclowns.